Three things you can't hide: The Sun, The Moon and The Truth." ~ Buddha. All that is needed for evil to succeed is that decent human beings do nothing ~ E Burke

BK Lim's Archive
macondo
  • Story Photo

    “One of the last areas that we went to was the rig floor, where they were already conducting the negative test. The first negative test,” Ezell said later. “And the tour group left and left Jimmy Harrell and myself there because they were having a little bit of a problem.”

    Ezell’s “bit of a problem” has since been described by BP as “a very large abnormality” in the pressure readings — most likely caused by gas building up in the well. Highly pressurized methane is almost always present in an oil formation, and if there were leaks or other defects in the walls of the well, this gas could seep in and build up to a potentially dangerous level. In extreme cases, if the pressure from the formation outside (and beneath) the pipe exceeds the pressure of the drilling mud or water inside the pipe, it can lead to a full-on blowout of the well.

    The decisions Harrell made next, and the subsequent ones made by the senior BP man onboard, Don Vidrine, would matter more than just about anything that had ever happened in the lives of the crew.

    If there is the possibility of a gas bubble, or “kick,” in the well, often the procedure is to recirculate all the mud in the pipe from bottom to top to clear out the gas, a process that takes hours. Instead Harrell, not sensing a crisis, chose a quick fix. He told them to bump up the pressure going to the blowout preventer, or BOP, a five-story stack of valves that sits on top of the wellhead on the seafloor and that is supposed to be able to stop a runaway well in an emergency. In a “well control situation,” as the oilmen refer to it, when pressurized oil and gas rush to the surface through the well, any one of the different valves in the BOP is supposed to be able to shut off the flow, the way the valve under a sink might be employed if the main faucet is broken. Harrell’s solution to the problems Wheeler and his crew were having didn’t really address why there might be an abnormally high amount of pressure in the well; it just cranked the faucet tighter, forcing the pressure back down the pipe, from 1,500 psi, which is normal, to 1,900 psi, which was high, but not dangerously so.

    Harrell’s solution worked — for half an hour, anyway, which was long enough for him to consider the test a success and for him to rejoin the visiting executives.

    Not everyone was sure that the problems with the pressure test had been solved, however — especially not Wheeler.

    “Wyman was convinced that something wasn’t right,” Christopher Pleasant, a subsea supervisor, recalled later. Pleasant had just arrived on the rig floor for the beginning of the night shift. “Wyman, he was still, like, shaking his head, he couldn’t believe it.” In part because of Wheeler’s unease, Vidrine and another BP rep agreed to repeat the pressure test. But as Wheeler had reached the end of his shift, this new test fell to Jason Anderson, one shift away from his 7 am helicopter transfer to another rig. Ezell asked if Anderson needed any help.

    “Why don’t you go eat,” Anderson told Ezell. It was now past 6 and Ezell was due in yet another meeting with the visiting execs at 7.

    “I can go eat and come back,” Ezell said.

    “Man, you don’t need to do that,” Anderson said. “If I have any problem at all with this test, I’ll give you a call.”

  • But that is not the only similarity with the Deepwater Horizon disaster. These drilling rigs are equipped with a general alarm designed to go off and signal an evacuation if two or more sensors are triggered within a zone. On the Deepwater Horizon, the general alarm had been intentionally “inhibited”, in essence, it was disabled for well over 8 months prior to the April 20th event. In the North Sea incident, alarms were also being continually activated until they were disabled as well.

    The main point that was addressed in the North Sea incident was lack of well control at the time of well completion when the drilling mud was being displaced with sea water. This situation was exactly the same on the Deepwater Horizon. Early in the day on April 20th a controversial decision was made by BP and agreed upon by Transocean to displace the drilling mud with salt water. This decision directly lead to the Deepwater Horizon disaster.

    So what went wrong with management? The North Sea incident occurred about 4 months prior to the Deepwater Horizon disaster. Transocean’s internal report on the incident was dated April 14, 2010 – 6 days prior to the disaster on April 20, 2010 in the Gulf of Mexico at the Macondo well.

    Had the report and subsequent recommendations from the North Sea incident been disseminated to the drilling management for the Gulf of Mexico operations, then it is likely that the Deepwater Horizon disaster would have been completely avoided.

    Transocean is the world’s largest offshore drilling company with three main divisions – North Sea, Asia and North America. It is management’s responsibility to coordinate the various activities under one’s charge. There is no excuse for poor coordination at management level especially when it comes to safety.

  • Story Photo

    The accident came as it emerged that two more people working on the clean-up have died, bringing the total number of fatalities since the Deepwater rig exploded on April 20 to 13.

    One of the latest casualties died while working on a vessel skimming oil.

    Before yesterday's accident with the cap, up to 60,000 barrels of oil per day were leaking from the oil well - that has now increased but it is not clear by how much.

    Coast Guard Admiral Thad Allen said an underwater robot bumped into the vent system before 10am.

    This sent gas rising through the vent that is supposed to carry warm water down to prevent ice-like crystals from forming in the cap.

  • Story Photo

    The Montara accident resembled the Gulf of Mexico accident in that both started with problems in the well itself, and it proved very hard to stop without resorting to further underground drilling, said Elmer P. Danenberger III, who was the top American regulator of offshore oil drilling until his retirement on Jan. 2.

    “There are clearly some similarities,” Mr. Danenberger said.

    Drilling the relief well proved tricky in the Montara spill, which was located in Australian waters in the Timor Sea, between northwest Australia and Indonesia.

  • Story Photo

    In summary, as at April 2009 when the H1 Well had been suspended and the West Atlas rig had departed from the Montara WHP to undertake other work, not one well control barrier in the H1 Well had been satisfactorily tested and verified, and one barrier that should have been installed was missing. In other words, the H1 Well was suspended without regard to PTTEPAA’s own Well Construction Standards or sensible oilfield practice.
    When the West Atlas rig returned to the WHP in August 2009 it was discovered that the 13⅜ ” PCCC had never been installed. The absence of this PCCC had resulted in corrosion of the threads of the 13⅜” casing and this, in turn, led to the removal of the 9⅝” PCCC in order to clean the threads. This was viewed by PTTEPAA personnel as a mere change of sequence that simply involved bringing forward the time of the removal of the 9⅝” PCCC. PTTEPAA’s Well Construction Manager, Mr Duncan, took a positive decision not to reinstall the 9⅝” PCCC. This meant that, according to PTTEPAA’s operational forecast and drilling program, the H1 Well would have been exposed to the air without any secondary well control barrier in place for some 4 to 5 days, with sole reliance on an untested primary barrier (the cemented 9⅝” casing shoe) that had been the subject of significant problems during its installation.
    After the 9⅝” PCCC had been removed, the H1 Well was left in an unprotected state (and relying on an untested primary barrier) while the rig proceeded to complete other planned activities as part of batch drilling operations at the Montara WHP. The Blowout in the H1 Well occurred 15 hours later.
    In the petroleum industry, well integrity is ensured by always having built in redundancies (secondary barriers) to safeguard against a blowout. Unfortunately, in the H1 Well there were no tested and verified barriers in place

  • As of Friday noon, large quantities of oil are still gushing into the Gulf, and the first slicks are starting to reach the many beaches along the mouth of the Mississippi. Estimates of the size continue to grow — now up to five times again as large as estimated just yesterday (25 times original 1000 bbls/day). See these amazing photos from the Boston Globe.

    We still don’t know what caused the blowout and explosion, but the Wall Street Journal is running a story suggesting the cause may have been related to the process Halliburton used for sealing the holes and gaps created during the drilling process.

  • BK Lim et al (revised 29 Jan 2012, updated 19 Feb2012 ).Credit due to Trisha James, Trisha Springstead, Jbao, Lambert & others for their contribution/updates.

  • Updates: This was originally drafted as part I but amended to part II based on feed backs from a closed group of followers. It was a question of presenting the facts first and the motives later or vice versa. The context of the article remains unchanged except for last minute inclusions.

  • Long Absence of BP related articles.

    Readers would have noticed the long absence of our BP Gulf disaster articles until recently in late January. We stopped writing about BP’s Macondo Blowout & mega oil spill disaster since early Sept 2011. Not because we had run out of issues to write. Not because the disaster and its environmental impact have fallen out of favor or out of the mainstream media’s focus. On the contrary, there was even more to write after an insider’s tip to http://oilspillhub.org. The website was registered on 21 June 2010, under Purdue University.

    Initially it was to concentrate on reviewing the long hours of the early videos. Then there was the cointelpro soon after revealing videos and snapshots were posted on cyberspace by various members of our circle. While the American public was demanding to know the truth of the disaster and the early videos of the accident (crime) scene, BP submitted (discreetly) the eagerly awaited videos to Congress. Why were these revelatory videos not released to the public in May 2010? BP obviously needed time to doctor the videos and to let public anger subside first. It works to their advantage if the truth is known later.

    Only when the lying stops can the healing begin.

    We need to keep the Gulf issues alive, not for any political or monetary gains but for the continuing long term damage to the world's environment and climate from the continuing leak (crude oil, methane and other hazardous gas) from the reservoir and vaporization of hydrate. Despite its far reaching consequences, the hypocrite world leaders continue to be silent and blind to the illegal and corrupt activities in the oil industry.

    Many have risked their lives, overcame tremendous odds and sacrificed hours of thankless unpaid tasks analyzing these ROV videos. Decoys have to be identified from the authentic. Doctored details distinguished from actual ground details recorded at site. Finally, we have to make sense of them all with respect to the time line of real events. To all those who had contributed their time, efforts and collaboration, we salute and thank you. Many more worked silently behind the scene to make these series of articles possible. Your contribution in helping to save the planet and the environment are beyond mere words of thanks and gratitude. With this introduction, we now turn to the second part of the series, “BP's Deception in the Gulf Exposed”.

    The other series “BP's killing spree in the Gulf” (dealing with long term environmental consequences of the Gulf disaster) and “The mafia in the global oil industry” (the crime of mass destruction and unscrupulous market manipulation behind these mega oil spill disasters) are in their final drafts and shall be released later under certain circumstances.

    There is little doubt BP needed to lie to cover the “hole”.

    What the public do not realize is the extend of the cover-ups to hide a really big hole. Not only did BP illegally and indiscriminately drilled 3 wells over a 7 month period, they intentionally blew up the last after fighting through hell to reach the reservoir at 18,360 ft bsl. To the sleepy ignorant world at large, it just does not make any sense. Why spend more than USD200 million just to blow it up? The Nazis burned down their own Reichstag in Berlin on 27 February 1933 for the same reason. Pearl Harbour was allowed to happen to get US into the war. 911 is now confirmed to an inside job. So was Fukushima 311, a deliberate crime of mass destruction planned Khazarian Satanists. Would the BP's Gulf disaster be any different, especially in the light of so many incriminating evidence?

    This disaster is one of the many, designed to push the world into global economic anarchy, mass destruction and catastrophic climate change. There is a lot of mis-information being floated in cyberspace to counter the truth and the real agenda of geopolitics and global control by the cabals. For more background information, please refer to articles by David Wilcock and Benjamin Fulford websites at these websites:

    FINANCIAL TYRANNY: Defeating the Greatest Cover-Up of All Time

    The real reason behind the 911 terror was a battle for control of the global collateral accounts

    BP’s Crime of Mass Deception. - 17 Aug 2010.

    Coincidence is the word we often use when we want to hide the truth and BP’s oil spill disaster has more than its fair share of coincidences. Matt Simmons’ death 2 days ago, is a great loss to all those seeking the truth. In one of his final interviews, Matt Simmons said, “It was painful as can be… to be the only person in the industry that was willing to speak out.” This article is dedicated to him and all living beings on earth that had been harmed by BP or agents employed by BP, in this crime of the century; BP’s Crime of Mass Deception.

    The failure of the latest “static kill” on the wrongly capped well (Macondo A) is the final nail on the head for BP’s crime of mass deception. This article is the first of several series that will present evidence of BP’s crime of mass deception for public discussion. Without doubt, underhand tactics and adulterated data would be used to discredit my articles and me as they had done on Matt Simmons. Self-serving bloggers would be employed by BP to disseminate distorted half-facts and confuse the general public under the guise of technical discussions. Do not be intimidated by technical jargons meant to confuse, for the truth is always simple and logical. There are no hidden motives in my series of articles other than to educate, disseminate the truth and point out the obvious flaws in BP’s crime of mass deception. My expertise in the field of geohazards geophysics, is given here on a pro-bono basis as part of my contribution to Mankind so that we need not live in fear of another man-made disaster.

    One will also need to understand the economics of deep water oil production, global market manipulations and super-quick financial windfalls from predetermined “natural or accidental” disasters. Our (ongoing) investigations led us to connections with other Inside-Job disasters like 911, 311, 26 Dec quakes in 2003,2004 and 2006 just to name a few.

    How did regulatory enforcement fail so badly? Gross negligence, cost cuttings and accidental mistakes were just the facade of an underlying sinister scheme. There is simply no excuse for the multiple blowout craters and gushing leaks over several tens of square miles on the seafloor. BP would have gone bankrupt in an instant once the world knew of the massive irreparable damage BP had done to the Gulf through their indiscriminate drilling activities. They wanted to short BP shares not kill it. Triggering a disaster was the easy part. Controlling the beast was another ball game altogether. BP had no idea how to kill the multi-head hydra monster unleashed from the deep. The easiest way out? “Fake and Confuse” strategy.

    How to convince the world that the oil had ceased leaking from the Macondo reservoir?

    The oldest trick in the world. If you can't make it, fake it. Using the “leaks on the riser” illustration enabled them to collapse the multiple leaks into one single leak at the shallowest well (A). Then when the time was right, they would do a “switcheroo” to well B. The gullible world audience would not notice the difference. They would even applaud the heroic battle. “A responsible global corporate kills the gushing beast”. That was the script until the late Matts Simmons (RIP) started to “pull the loose thread” from the flawed knitting. In his previous capacity, he served as energy adviser to U.S. President George W. Bush. He was, up until his death, a member of the National Petroleum Council and the Council on Foreign Relations. JP Wheeler was another of former Bush Administration adviser who was found dead in a dumspter on 2011 New Year Eve. Like Simmons, he too had to be killed for knowing too much.

    The late Matts Simmons was killed days after their attempt to seal the third well (labelled as well BE) failed.

    Contrary to BP's denials and Rtd Adm Thad Allen's incomprehensible explanations, Relief well C intercepted the rogue well at 18,000ft as early as the first week of July 2010. With an operational cost of 1 million USD per day, why would Relief Well C be “playing footsie” at less than 20ft from the rogue well and did not intercept for more than 2 months? It is like saying “I smoke marijuana but never inhaled”. BP could get away with such blatant lies because no one dared to question stupidity. Direct access to White House helped.

    After multiple failures to stem the gushing flow and out of sheer frustration, an explosive device was detonated at around midnight (local time) on 1Aug 2010 in an attempt to bottom kill the gushing well. It was no coincidence an abnormal 3.0 mag shallow quake struck Louisiana at the same time. The epicentre of that rare shallow quake plots on the same NW-SE fault line which also ran through the “gas bubble” discharge noted on the evening of 22 April (1744 CDT). That shallow gas eruption was induced by an earlier shallow depth detonation within the same Macondo well. It makes perfect sense for a detonation at depth of 18,000ft (5.5km) bsl to trigger a 5 km deep quake more than 200 miles away. And a shallow explosion <6,000ft (1.8km) bsl to induce a shallow gas surge 50 miles away along the same fault line. You cannot get a better correlation than that.

    Apparently, the 1st Aug bottom-kill attempt was not that successful. BP had to abort its scheduled “show killing of well A” in early August. The rogue well started spewing again. Incomprehensible announcements were made on the deferred well killing. The late Dr Manton was silenced with a 15-year jail sentence 5 days later, followed by the late Matts Simmons drowning in the bath tub incident and the late Senator Ted Stevens' plane crash, 2 days apart of each “accident”. The odds must be astronomical for each of these incidents to occur accidentally and independently of each other.

    Silencing The Independent Voices Of Truth On The Bps Mega Oil Spill Gom

    Implication Of Dr TB Manton's False Conviction And Murder

    Miscalculations were probably at fault. Or was it Divine intervention? Both detonated events (22 April and 1Aug) did not yield the expected results. “Man proposes while God disposes” does sound sweet. After the anticipated massive oil spill failed to materialize on 20 April, they were under even more pressure to make it right (sounds familiar to BP's pledge?). They could not afford to take any more chances.

    A disastrous gas blowout with no massive oil spill does not move global markets and oil prices. On the other hand, an anticipated mega oil spill that did not happen at the right time could spell financial ruins as huge bets had been placed to make the huge killings. The markets had to be caught by surprise. With mounting losses from a series of “failed-to-materialise” disasters, they had to make or break. Does the determination to cause a mega oil spill make any sense now?

    The mega oil spill has other sinister agenda as well. A deceptive slow-killing cancerous genocide is more profitable and provoke less public outcry than an outright genocide. Depopulation agenda come to mind.

    The detonated explosion on the evening of 22 April had to be powerful enough to breach the base cement plug to achieve their ultimate objective. No second chance. Too much was at stake. If you can predict the weather, the market is yours for the taking. Like a rigged horse race, a mega oil spill in the gulf had to happen to avoid financial ruins. If the Let-It-Happen-On-Purpose (LIHOP) did not work, they had to resort to Make It Happen On Purpose (MIHOP). But each backup action leaves its own trail of incriminating evidence. Investigators obviously did not seek to find.

    The many financial bubbles (eg 2007 Sub-prime and Housing Bubbles) and the 2008 Global Financial Meltdown were no accident. So were the top hole blowout at 2200CDT April 20 and the more disastrous bottom hole blowout shortly after 1700 CDT April 22. Deception works best when the evidence are shown right under our noses. Many examples were given in part 1 of this series, The Farcical 3 Leaks On The Broken Riser Story.

    Distorted truths are most dangerous when they appear to be the whole truth.

    Deception fools no one if the distorted truths are not publicly disseminated. Hence the need for “independent witnesses” (another name for agents or schills) to spread these distorted truths. Any wonder BP spent 3 times than normal (>$100 millions) in the months following the outbreak of the disaster?

    Every discrepancy is a window of opportunity to seek the truth. The truth will not falter despite the many spanners thrown at it. Followers to our articles would have known the number CoIntelpro operations used to disrupt our independent investigation. There has been useful insiders' information and tips as well. We have grown wiser to their deceptive tactics and mis-information. Our sincere apologies if some of the insiders' leads were not followed up promptly.

    We received many leads on the timing of key events like the “Second Underwater Explosion” (SEU), sinking of the Deepwater Horizon (DWH) and discrepancies in the various logs (mud logs, US coast guards, well activity logs etc). Due to limited resources, various tasks had to be farmed out to volunteers. This article was prepared before we have received all the feedbacks. This jewel of discrepancies among the early responses to the blowout and rig fire is a last minute inclusion to this article.

    Were the US Coast Guards notified of the explosion on DWH 3 hours before BP reported event at 21:49 CDT?

    One keen investigator highlighted an apparent time discrepancy in some of the events found in the USCG log.

    A. 202357Z APR 10 (18:57 CDT 20 Apr 10)

    INITIAL CIC BRIEF// D8 RECVD DSC FROM MOBILE DRILLING UNIT DEEPWATER HORIZON OF AN EXPLOSION ON BOARD. THERE WERE 144 POB. CAUSE OF EXPLOSION UNKNOWN. THERE IS A 285' WORKBOAT AND 2 LIFE RAFTS ON SCENE. 87 POB HAVE BEN RECVD AND ARE ON THE 285' WORKBOAT. 2 H-65'S FROM A/S NOLA, H-65, H-60 AND C-144 FROM ATC MOBILE LAUNCHED AS WELL AS CGC POMPANO AND CGC RAZORBLEL. SEVERAL GOOD SAM'S ALSO RESPONDING. THE RIG COMPANY IS TRANSOCEAN; D8 IS TRYING TO GET MORE INFORMATION FROM THEM. RIG WAS 72NM SE VENICE LA IN POS 28-44N 088-21W. // FOLLOW UP CIC WILL BE AT 0445Z.

    E. 210303Z APR 10 (22:03 CDT 20 Apr 10)

    INITIAL NOTIFICATION. D08 RCVD DSC ALERT FOR THE MODU DWH 45NM ESE OF SOUTH PASS LA. RVCD CALL FROM A RIG 25NM AWAY FROM THE DWH MODU IS ON FIRE AND THERE ARE PERSONS JUMPNG INTO THE WATER AND THEY ARE SENDING 5 VESSELS TO ASSIST. D08 LAUNCHED A/S NOLA A AND B CREWS AND CL44 FROM ATC ALSO REQUESTED ADDITIONAL CREWS.

    H. 210306Z APR 10 (22:06 CDT 20 Apr 10)

    SECTOR RCVD GOODSAM CALL FROM THE M/V RAMBLING WRECK RELAYING COMMS REPORTING THAT THE RIG DWH IS ENGULF IN FIRE AND PERSONNEL ARE ABANDONING THE RIG.

    Note: CDT time difference with Zulu time (denoted by Z in the USCG logs) was assumed to be -5 hours. We had to use our best discretion when no “z” was indicated. BP also had a complete blackout of independent sources of confirmation. Unfortunately we cannot reveal our sources and ingenious means of verifying the truth.

    Item A at 202357Z Apr10 (18:57 CDT) was 3 hours 5 minutes earlier than the mayday distress call sent out from DWH. Item E at 210303Z Apr10 (22:03 CDT) apparently sent from a rig 25nm from DWH (Matterhorn MC243 operated by W&T offshore) was 11 minutes after DWH's mayday call at 21:52 CDT or 14 minutes after DWH was engulfed in flames from multiple explosions at 21:49 CDT. Nakika platform is nearer at less than 15nm but operated by BP. Item H 22:06 CDT was a call received from a good samaritan vessel in the vicinity (about 15 minutes away or less than 5 km with maximum speed of 10 knots) of DWH. The first USCG helo arrived at 23:22 CDT (or 1 hour 20 minutes after the distress call was picked up) according to BP's official report. Why was there a 4-minute delay between the blowout (21:45) and fire (2 explosions at 21:49) and another 3 minutes before Mayday call?

    How did Anchorman know that all personnel abandoned rig 10 minutes after mayday call at 21:52 CDT at that time, 10 miles away? Why did it take more than 10 minutes for the Matterhorn platform to relay the distress call to D8? Why didn't the BP-operated Nakika platform pick up the distress call 15nm away and relay it drectly to BP or Transocean, under their Emergency Response Procedures (ERP)? It would presumably take less “fumbling time” than Matterhorn platform (which is still no excuse). Yet Anchorman, an independent witness could pick up the “event (@21:45)” 10 minutes before the mayday call; a full 20 minutes ahead of Matterhorn's distress alert.

    The first public blog reporting on the DWH rig fire (by anchorman on Gcaptain.com) was 21:34 (-6 hours or 22:34 CDT) or 45 minutes after the official Mayday Call from DWH. Anchorman was just 10 miles away but was stuck on anchor. No reasons or explanation were given.

    At 12:27am (1:27 CDT 21 April) 2nd posting by Anchorman:

    We are 10 miles away, but we are stuck on an anchor and ccan not assist. This happened @ 2145. Ten minutes after the mayday, they abandoned ship and the flames were at least 200' tall. It's still raging and it's 0130 in the morning now. I called Transocean when it happened and they were not aware, but the Coast Guard just called them, I updated them. So, I gave them my assessment. Several vessels are conducting search patterns at this time. The head count on the rig was reported to be 129, but there has not been a hard count on the radio. We are going to the location within the hour. http://gcaptain.com/forum/offshore/4805-deepwater-horizon-transocean-oil-rig-fire.html

     What is wrong with this first response scenario? More detailed analyzes would be coming out of Lambert's investigation later but at this preliminary stage, the conspicuous absence of both BP and Transocean was just too “loud” to miss. Why?

    It is mandatory for BP and Transocean to have manned shore control stations / operation managers on 24/7 standby basis. Any mayday call from their own rig would have been picked up in a matter of seconds. So why would Transocean still be unaware at least 12 minutes after the mayday distress call was sent out. Never mind the developing trouble on the rig as early as 21:45 CDT when the assistant driller called the senior toolpusher to report that the well was blowing out. Like any expecting father, the operation managers at BP and Transocean shore control would be glued to the radio, closely following the operations in the final hours before DWH pulled out from a “strike well”. For BP and Transocean to be caught unaware of the impending troubles on DWH would be complete lunacy. 

    Were BP and Transocean caught sleeping on the job or was it part of the contrived plot to blow up DWH?

    Were BP's and Transocean's 24/7 manned shore control stations sleeping on the job? Then what about BP-operated Nakika platform? Were they sleeping on the job too? Hardly. If you are contriving to blow up your own rig, you too would make a conscious effort to avoid being mentioned in any document that could be construed as a scripted plan, just in case it falls into the wrong hands. The conspicuous absence of BP and Transocean is a major flaw in the plot since in any accident on the rig, the owner-operator (Transocean) and the Client (BP) would be the first to be notified. Thus in the scripted plot, everyone else was aware of the fire except BP and Transocean as if to distance themselves from the “ACCIDENT”.

    It is not known if Anchorman (a vessel captain working for Pacific Drilling) had “superman vision” to pierce through the darkness and steel walls, to be able to see and count all the personnel who had abandoned rig (jumping into the water or with life rafts). Yet for all his superman abilities, he was wrong on the 129 POB, “all had abandoned ship” and “drilling ship” information on his posting and could not pull off anchor 3 hours 42 minutes later. Why had all the investigations ignored Anchorman's eye-witness account of the incident?

    See Anchorman's eye witness account of DWH's explosion / fire 10milesaway.

    Assuming Anchorman was an independent observer minding his own business 10 miles away from DWH, what was his vessel doing at anchor 10 miles from DWH? Was his vessel one of the passing good Samaritans mentioned in the “scripted plot”? If his vessel was anchored so close to DWH, there would have been radio contact prior to the blowout (accident) since vessels in the vicinity of any platform or semi-sub rigs would need to identify themselves as part of the security measures against untoward accidents or unwelcome activities. As an experienced skipper, he should have known the difference between a drilling ship and a semi-sub rig. The fact that he could report the burning vessel as “Deepwater Horizon” meant that he knew. So why the deliberate “abandon ship” instead of “abandon rig”? Then again how did he know the accident happened at 21:45 CDT and all the personnel had abandoned “ship 10 minutes after the mayday”. Mayday call was sent out only at 21:52 CDT. An independent witness could not have known such precise details, not at that time and certainly not in the darkness 10 miles away.

    Anchorman posting on Gcaptain.com at 1:27 CDT (3 ½ hours later) wrote “I called Transocean when it happened and they were not aware, but the Coast Guard just called them, I updated them. So, I gave them my assessment.” In his first posting at 22:34 CDT, his exact words were “The Deepwater Horizon is on fire and the flames are 200 ft tall. All personnel have abandon ship.”

    This is most surprising. Did he call Transocean shortly after 21:45 CDT the time of the blowout or after the mayday call was sent out at 21:52 CDT? Both would indicate Anchorman had prior knowledge of the blowout before it happened. If D8 was notified at 22:04 CDT, why were BP and Transocean still in the dark about the “Accident” on their own rig more than 12 minutes after the mayday call was sent out? Surely offshore regulations in the US cannot be less stringent than 3rd world countries.

    Were BP and Transocean really sleeping on the job or was there a contrived plot to blow up DWH?

    Does the phrase “crude corruption and oily business” come to mind?

  • Story Photo

    Uploaded by ABCActionNews on Jul 23, 2010

    Chemical tests confirm two plumes of oil beneath the surface of the gulf came from that BP broken well.

  • Story Photo

    In September 2009, two time-series sediment trap and current meter moorings were deployed in the northern Gulf of Mexico to investigate biogenic fluxes settling to the seafloor (and larval recruitment) at two well-characterized and significant sites of combined deep-water coral and chemosynthetic tube-worm colonies (Fisher et al., 2007). Each of these traps, set just above the seabed and in water depths of 400-450m, have been collecting a new sample of settling material every two weeks since 11 September 2009 and will continue to do so until 2nd July 2010 when their last sample bottle will be rotated shut and the traps will await recovery as part of an already-funded field program (NOAA-MMS) scheduled for November. Serendipitously, however, these two traps are located just 32 nmiles to the NE and 81 nmiles to the WSW of the recent Deepwater Horizon incident and continuing oil release from the seafloor. Continuous monitoring by NOAA has shown that at least one of these two study sites became overlain by oil discharge at the ocean surface by the end of April and that both sites are now overlain by at least light to medium concentrations of hydrocarbons ± dispersant. What remains unestablished at this point, however, is what is happening at depth and what impacts there may be at the Gulf of Mexico seafloor and, specifically, its pristine and unique deepwater coral/ chemosynthetic tube-worm colonies. The purpose of this proposal, therefore, is two-fold.

  • Story Photo

    Please submit your favourite quotes of this disaster (that make you want to vomit blood, pun intended) to be included in the "Quotes of Shame - BP Gulf disaster". To be published on the 2nd anniversary of the disaster.  

  • Story Photo

    Uploaded by WalKnDude002 on Jun 27, 2010

    COREXIT is Eating Through Boats in the Gulf

    http://www.youtube.com/user/o0Levitikuz0o

    Corexit has started eating through boats in the Gulf . . . BP told the EPA "to stuff it" over the use of Corexit, which was found to be 4 times more toxic than the oil itself. BP is also in control of the U.S. Coast Guard which has threatened reporters with arrest that have gotten to close.

    Music Produced by: 2Deep - Just Another Day

    This video is for educational and news purposes only, which is protected under sections 107 through 118 of the copyright law.

    Kid with oil stuck on her Destin Beach Fl June 23rd 2010 Oil Rain Louisiana River Ridge Bp CNN almost all exxon valdez cleanup crew dead Kindra Arnesen Venice LA Needs to Evacuate BP Spill Environmnetal Disaster Fishing Industry health risks Chemical in South Carolina corexit dispersant toxic blocking blocks media access new orleans

  • Story Photo

    Real BP America
    The speaker from the USCG at one of the meetings said the same thing David said. He actually asked me would I rather have seen no Corexit being sprayed and dealt with the consequences. I said a firm YES! At least then we could have dealt with it out in the open and gotten rid of it. Then he went on about how he was exposed to Agent Orange in Vietnam and that this stuff was nothing compared to that. At that point, I realized talking to them anymore was pointless :-(

    Tuesday at 10:26am · Like · 1

  • Story Photo

    Tens of billions at stake in BP oil spill trial

    By Mira Oberman (AFP) – 11 hours ago

    CHICAGO — Tens of billions of dollars will be at stake when BP heads to a US court this month to determine how much it owes for the massive Gulf of Mexico oil spill and how much it can shift to subcontractors.

    Several government probes have castigated BP, rig operator Transocean and Halliburton -- which was responsible for the runaway well's faulty cement job -- for cutting corners and missing warning signs that could have prevented the disaster.

  • Gold in free fall - 20% down from high – September 26 2011 at 06:21pm

    The gold price is in free fall and only another major global crisis will stop its descent.

    After falling 11% last week, the precious yellow metal dropped 7.5% on Monday - its steepest one-day fall in five years - bringing the gold price down 20% from its all time high of US$1,920.30 an ounce in early September.

    This makes this month gold's worst month in three years.

    By late afternoon, the precious metal had lost almost US$50 from the US$1,641.39 it was quoted at the JSE's close on Friday to trade at US$1,591.50 - some US$328.80 from its all time high.

    Many market watchers warned that a correction was coming and now they are saying the price is likely to bottom and level off before it starts to climb again.

    “Gold has certainly taken a dive - and could stumble further in the days immediately ahead - but I think we will see the yellow metal begin its comeback sooner rather than later, possible in the next few days,” said Jeffrey Nichols, managing director of American Precious Metals Advisors.

    While the threat of another global economic meltdown has not been dismissed, the US dollar is the sweetheart of investors. In times such as these, the US dollar does then reign supreme. It should and it shall. 'Money' is finding its way to its ultimate safe harbour, and clearly that is not the euro and that is not gold,” said Dennis Gartman in Monday's Gartman Letter.

    Wasn't the financial world predicting the demise of the USD since the 2008 financial and economic crisis and collapse of Lehman Borthers? With an imminent Greece Default on the line, to be followed by successive PIGS defaults, US and its European allies controlled by the cabal at their wits' end with their backs to the corner. Was this report timed for release on September 26 2011 for financial gains? The numbers 26, 11 and month September seem to be appearing in many suspected inside jobs or planned disasters. Are these numbers accidental or timed as in setting one's alarm clock?

    Cabal resorting to desperate tactics as they try to prevent reboot of financial system

    There are many signs available in both the corporate propaganda media and the people based independent media that some sort of end-game crisis is approaching for the criminal cabal in charge of the G7 countries and their shrinking coterie of slave states. With the Pentagon and the Russian military aligned against the cabal, their downfall is close. For that very reason the cabalists are attempting to stage some sort of game changing atrocity, probably in either the US or Europe. ~ Benjamin Fulford.

    Is the old financial world long dominated by the cabalists at the brink of collapse? A world war (WWIII) involving the major creditor countries would solve the headaches they are having right now. It is not they haven't not tried. The Bush-Dick Cheney Administration had been trying to ignite a full blown world war after faking the 911 (Bush's Pearl Harbor) attack and blaming it on the Saudi patsies. Incidentally, the first plane crashed into Tower One at 8:46 am on American Airline flight 11. United Airline Flight 175 crashed into Tower 2 at 9:03 am, 17 minutes later. American Airline Flight 77 crashed into the Pentagon (5) at 9:37am or 51 minutes after the first crash or 34 (17x2) minutes after the 2nd. Two as in double 7. A fourth (4) flight, United Airlines Flight 93, under the control of four (4) hijackers, crashed near Shanksville, Pennsylvania, southeast of Pittsburgh, at 10:03 a.m; exactly 1 hour after Tower 2.

    Japan's worst nuclear-tsunami-quake (3 as in triple) environmental disaster struck on 3-11-11 at 14:46 JST (05:46 UTC) or amazingly, 11-3-11 at 00:00:46 EST. The magnitude of the quake was 9 approx 70 km (or 43 miles which numerologically adds to 7) east of the Oshika Peninsula of Tōhoku. This disaster was dubbed Japan's 311, 10 years after 911. Was Japan's 311 timed to occur exactly 46 minutes after the hour as the 1st plane did?

    If you think these are just coincidences, look at 3 other earthquakes suspected to have been triggered.

    The 2003 Bam earthquake (1226) was a major earthquake that struck Bam and the surrounding Kerman province of southeastern Iran at 1:56AM UTC (5:26AM Iran Standard Time) on Friday, December 26, 2003. The most widely accepted estimate for the magnitude of the earthquake is a moment magnitude (Mw) of 6.6; estimated by the United States Geological Survey. The shallow earthquake (10 km) was particularly destructive, with the death toll amounting to 26,271 people and injuring an additional 30,000. - wikipedia.

    The 2006 Taiwan major earthquake (1226) occurred 90 km (55 miles) SSE of Kao-hsiung, Taiwan and 795 km (495 miles) N of Manila, Philippines at 6:26 AM MDT, Dec 26, 2006 (8:26 PM local time in Taiwan). Depth: 10 km. USGS public info.

    Both the 2003 Iran and 2006 Taiwan quakes were timed to destruct at precisely 26 minutes after the hour, exactly 3 years apart. The 2004 Indonesia quake which occurred 1 year after the Iran quake, had a disputable magnitude of 9.1 to 9.3 . BK Lim ( Bush lied on USS-San-Francisco-Accident) tied the 2005 January 8, 11:43 GT San Fran accident to the 2004 December 26 quake which happened at 10:58 GT, 13 days earlier.

    The 2004 Indian Ocean earthquake was an undersea megathrust earthquake that occurred at 00:58:53 UTC on Sunday, December 26, 2004, with an epicentre off the west coast of Sumatra,Indonesia. The quake itself is known by the scientific community as the Sumatra-Andaman earthquake.[3][4]  - wikipedia

    Compare this with the timed events on the Macondo BP Blowout (20100420 Bp-Oil-Spill-DWH Timeline).

    18-Apr-2010 20:58 (8:58pm)

    Partial lab test results, a new OptiCem™ model report (using seven inline centralizers) and Halliburton’s cementing recommended procedure for the Macondo well cement job were provided to BP and Halliburton staff. [Complete lab test results on planned slurry design not provided to BP before job was pumped.]

    Email from Halliburton inhouse cementing engineer to BP and Halliburton staff

    (same minute as 2004 quake)

    20-Apr 2010 (21:46) 9:46 pm

    ~21:46 hours—Gas hissing noise heard and high-pressure gas discharged from MGS vents towards deck.

    Real-time data Interviews MBI testimony

    (same minute as 911, Japan quake)

    20-Apr 2010 (22:00) 10:00 pm

    Explosion and Fire

    Transfer of 115 personnel, including 17 injured, to M/V Damon Bankston. 11 people were determined to be missing, and search and rescue activities ensued. U.S. Coast Guard arrived on-site at 23:22 hours.

    MBI testimony

    (coastguard arrival same as the minute DWH sank suddenly)

    22 Apr 2010 10:22

    Reported 2nd Explosion underwater. Deepwater Horizon sank.

    Unified Command

    Were all these events perfectly timed?

    The chance of 3 independent events happening within the same minute of the hour is 1: 216,000. At 8:46 am 1st plane crashed into Tower 1 on 911, Japan's 311 struck on 3-11-11 at 14:46 JST and the “high-pressure gas discharged from MGS vents towards deck” (a mistake?) at 9:46 pm. With astronomical odds like these, it would be a better bet to place your money on a “central command” behind the planning of all these disasters.

    The chance of 3 independent quakes (2003 Iran, 2004 Indonesia, 2006 Taiwan) happening on the same day of the year is 1: 48,627,125. The chance of 2 independent quakes (2003 Iran, 2006 Taiwan) happening on the same day of the year within same minute of the hour is 1:479,610,000.

    Compare the 2004 December 26 and a later quake on 2005 March 28 at around the same epicentre offshore Sumatra. You get the picture between a naturally occurring disaster and a triggered one.

    An excellent write up by Arjuna on Nuclear bomb caused the 12-26-04 Asian tsunami .

    Sumatra Quake: 28 March 2005

    Magnitude_8.7_earthquake_hits_Northern_Sumatra,_Indonesia

    A magnitude 8.7 earthquake has been reported in northern Sumatra, Indonesia by the U.S. Geological Survey (originally an 8.2 magnitude at 2:37 ET (7:37 GMT) the USGS reclassified it to an 8.7 magnitude). Government spokesman Agus Mendrova reported more than 290 deaths on the island of Nias. Hundreds of others were reported trapped in collapsed buildings, including structures weakened by the December 26th earthquake.

    A destructive wave was intially feared and many nations issued tsunami warnings. After the quake a USGS instrument near the Cocos Islands recorded a tsunami type wave which the USGS classified as "small." Tsunami warnings were later withdrawn.

    The quake occurred at 11:09 ET (16:09 GMT), and is considered a "great" earthquake, the largest of seven grades. This earthquake is also classified as a "shallow" earthquake, occurring within the top 50 kilometres of the Earth's crust. Shallow earthquakes are more likely to cause a tsunami, because as the lower within the surface the earthquake occurs, the less warping of the ocean floor occurs. This earthquake was a thrust quake; the December 26th Indian Ocean quake was considered a megathrust quake.

    Giant tsunami waves (>10m) cannot result from chaotic mass displacement of water. A high school physics experiment in creative and destructive wave motion, can prove this. Giant tsunami waves are created from well-timed creative wave sequence. “Destructive waveforms from chaotic mass displacement” is the norm.

    To create mega-tsunami, you cannot use HAARP or a single large nuclear explosion since there will always be random destuctive interference waves. You need carefully timed sequence of explosions. You can demolish a building with a single blast but the demolition will be unpredictably chaotic. You have modern controlled demolition experts for the job. I believe the 2004 Indonesian and 2011 Japan mega tsunamis were initiated by well-calculated controlled sequence of explosions to take advantage of a quake-prone situation. This was confirmed by the 8.7 mag quake on 28 March 2005 (3 months later) at approximately the same location as the 1226 Sumatra Quake on 26 December 2004.

    There is no financial benefit to a disaster you cannot time and control. The windfalls are obvious if you can accurately predict the time of these disasters. It is like rigging the roulette table. Similarly a financial tsunami can only be generated by a series of well-timed controlled (not chaotic accidental) events and disasters.

    What did GoldmanSachs know before the BP Blowout, to have sold 44% of its BP stock 3 weeks before? Tony Hayward sold 1/3 of his BP shares 1 week earlier. So did four other BP directors. What did these priviledged few know? Should those who profitted from through planned disasters or inside jobs, not be prosecuted?

    http://www.dailypaul.com/136466/goldman-sachs-sold-44-of-its-bp-stock-three-weeks-before-the-oil-rig-disaster

    www.telegraph.co.uk/finance/newsbysector/energy/oilandgas/BP-chief-Tony-Hayward-sold-shares-weeks-before-oil-spill

    Continue reading this entryContinue reading this entry ...

  • Story Photo

    Uploaded by OilFlorida on Aug 20, 2010

    Gulf Oil Spill and Seafood Safety Government Panel, House Committee Energy & Commerce, Energy and Environment, August 19, 2010:

    Edward Markey (D-MA), Subcommittee Chairman

    Bill Lehr, Senior Scientist National Oceanic and Atmospheric Admin., Response and Restoration.

  • Feb. 13 (Bloomberg) -- Transocean Ltd., owner of the rig that exploded before the worst offshore oil spill in U.S. history in 2010, sought to force a BP Plc manager to explain what occurred at the well prior to the blowout.

    Transocean asked the U.S. District Court in New Orleans to compel Donald Vidrine to testify. He was BP’s well site leader on the Deepwater Horizon rig when the Macondo well in the Gulf of Mexico exploded. Vidrine has cited medical-related problems for refusing to testify, in person or in writing, Transocean’s lawyers said in a court filing yesterday.

    Vidrine “is a key source of information regarding critical events and operations that occurred immediately prior to the blowout,” Transocean said. “Mr. Vidrine’s medical issues do not provide a legal basis for his refusal to testify.”

  • Story Photo

    Uploaded by KeepItTrillBlog on Jun 4, 2010

    Physics professor and author Michio Kaku speaks about the idea of nuking the Gulf oil well leak, on Keith Olbermann's show, 6-03-2010.

  • Story Photo

    But now in the Gulf, in the midst of a switchover process that calls for drastic depopulation, motive clearly enters the picture. What better way to move the project forward? Whatever toxic brew they cook up in the Gulf will be spread by the Gulf Stream all over the Atlantic Ocean and coastal areas, and into the global current system. And when the hurricanes begin, which they soon will, the toxic brew will be sprayed all over the Gulf region, making large areas of the coastal states, and probably all of Florida, uninhabitable and toxic to crops and creatures.

    And it is indeed a toxic brew. They tapped into a major migration channel of abiotic oil, deep down at the level where volcanos originate, and all kinds of toxic gases are being released along with the oil, under enormous pressure that cannot be contained and is leaking out from many places in the Gulf. And in case that's not toxic enough, they're adding all that Corexit, a neuro toxin banned in Europe because of bitter experience with its toxicity.

    None of this can be chalked up to accident. The geological properties of the area, and the nature of the deep oil system, were well known to the experts. The Gulf is one of the oldest and most studied drilling areas in the world. Any legitimate attempt to tap into that deep oil system would have called for better-than- usual safety measures, not systematically shoddy safety measures. Deep Water Horizon was an accident meant to happen, and the witnesses have been scared into silence.

  • Story Photo

    BP's 3 leaks on a single riser were not only ridiculous but impossible.

    BP claimed the first leak(1) was at the kink of the riser (bent riser) on top of the 70ft blowout preventer (BOP). BP admitted that most of the oil was gushing out into the Gulf was from the secondary leak (2). The smaller gas leak at well A could not be capped until the real rogue well (BE) aka leak(2) was sealed or bottom-killed 18,000 ft bsl (reported since July 2010).

    The third leak (3) was a just puny gas leak flowing out of the open end of a drill pipe. Figure 165-0 gives the various schematic illustration of the 3 leak points on the riser, based on BP sourced information. Besides adding the labels for clarity, the only other item added to figure 165-0a was the NW SE fault line. This fault line, as we shall see in later articles, was the critical factor in the shallow gas problems encountered in all the 3 wells.

    Simple logic dictates that it was physically impossible for these 3 leaks to occur on a single riser from a single blowout. Certainly not the way BP explained it. Figure 157 in Another Physical Impossibility 2 Leaks On The Broken Riser gave some of the discrepancies noted on Leak(1) and Leak(2) as early as Aug 2010. Note that leak(3) was allegedly sealed by capping the open ended drill pipe. Later articles will also show how BP tried to buy time by going through the charade of junk shot kill, top kill, top caps and giant domes etc, while the teams on site set up another BOP and reattached the Bent Riser at well A, to start the “dog & pony show” from mid May of 2010 onwards.

    In addition to the 6 discrepancies found in comparing leaks (1) and (2) in figure 157, here are a few more:

    The open ended 5½ inch drill pipe at leak(3) is of different physical dimension from the pipe (casing) at leak(2) and the Bent Riser on top of the BOP at leak(1). See the marked differences in figures 165-1b and 165-2.

  • At leak(3) the 5½ inch drill pipe should have been inside the 21 inch main riser pipe with the attached Choke, Kill, booster and hydraulic supply lines. It is physically impossible to explain how a long “naked” drill-pipe could have been stripped off its 21-inch Riser pipe casing at the mid-section of the riser string. More impossible still was the fact that it was sticking vertically out of the seabed with the weak gas plume. The naked standing drill-pipe could only be possible if it was ejected from the blown well itself.

  • If the riser was carrying the same drill pipe string (5000 ft long), how did the pipe at leak(2) suddenly become several times larger than the drill pipe shown at leak(3), immediately after the blowout?

  • In comparison with the other broken segments of the riser string lying on the seafloor, why was leak(2) so special and different if it was also broken from the same riser string? Fact: leak(2) could not possibly be from the same riser string.

  • BP claimed that leak(3) was sealed by capping the drill pipe. Why couldn't the drill-pipe within the riser at leak(2) be similarly capped? There were many reasons they couldn't. The main reason? Leak(2) was the blown crater of well no. 3 (well BE) and not the broken riser carrying the drill-pipe within.

  • Leak(3) was undeniably an open ended disconnected pipe just as leak(2) was. There could only be one severed open end in the riser segment still connected to the BOP. It can only be leak(2) or leak(3) and not both.

  • How did the oil “jump” across leak (3) and continue to flow to leak (2) as illustrated in 165-0a and b?

  • The later illustration (165-0c) corrected the leak(3) anomaly by placing it after leak(2). Only problem then, how do you explain the “open ended pipe” at leak(2)?

  • Figure 165-2 and BP's investigation report confirm that there were two 5½ inch drill-pipes within the Bent Riser. This means that the drill-pipe string within the riser was already disjointed near the BOP. How could oil/gas flow through a disjointed drill-pipe to leak out at leak(3) more than 500ft from the BOP?

  • The black oil plume at leak (2) was obviously more voluminous than the lighter orange-brown gas leak at leak(3) or leak(1). The color of the oil / gas plumes is consistent with the differences in the flow rate and volume noted in all the three leaks. Fact: the leaks are from different ground sources.

  • The videos show that the riser string was completely severed at several points and all the severed sections showed no gas/oil leaks. If Leak(1) was on the same riser string as leak(2) and leak(3) why was it not showing any oil/gas leaks until after mid May 2010 (more than 20 days later).

  • The earliest video on 23 April 2010 clearly showed a steep sided blowout crater with no “surface” riser going into the crater. The oil spewing pipe at the base of the deep crater, had to originate from the well below. With no visible supply of oil (through the surface riser), the obvious oil supply had to be vertically beneath the crater. This further confirms that leak(2) was the blown third well (BE). See the close-up view at figure 165-5.

  • The bent riser on top of the BOP was not leaking at all in the early videos before BP publicly broadcast leak (1) in mid May (20 days later). If leak(1) at well A was the primary leak, it does not make sense to show the secondary leak(2) first. Not unless the primary leak(1) at well was non-existent and had to be set up first?

  • Setting up well A as the “primary leaking well” was not in the original plan. It was a backup plan. This explains the more than 20 days media blackout on the supposedly primary leak(1).

  • The riser piping could not have bent and twisted like a pretzel and yet still remained intact, as the astonished experienced driller from Drilling Ahead believed (more of this later).

  • The riser string did in fact break at several places as seen in figures 165-1a and 1b. Again how could oil flow through these “severed discontinuities” in the riser? Fact: There was no oil flow as the ROV inspections showed.

  • The clearest evidence is the photo-shot of the vertically standing riser section (speared into the seabed). There was no oil spill emanating from it or in its vicinity. This clearly refutes the ridiculous official story that a neutrally buoyant riser with floats could dig itself beneath the seabed (like a buried pipeline) only to spew out the oil hundreds of feet away. Physics of Impossibility does not get more ridiculous than that.

  • If the well was already gushing out oil from the instance of the first blowout on 20 April 2010 (reported by BP to fuel the rig fire) why was there no immediate oil spewing out of the broken riser as it was sinking. The rig fire was in fact fed by more than 700,000 gallons (60% of max capacity) of diesel stored onboard the rig. Why was more than 60% of fuel still onboard the rig at the end of its long 3 months drilling campaign? Why was BP so certain free flowing crude from the well was fueling the rig fire without evidence?

  • It is now confirmed (see figure 165-3) that it took less than 16 seconds to fully bend from an upright (slightly inclined) position. The DWH (falsely reported as having sunk at 10:22 CDT) could not have sunk 5000ft to the sea bottom within a minute. Thus the riser pipe had to be deliberately broken near to the BOP; possibly less than 1000ft. Otherwise how could a marine riser which could withstand 80 mph Hurricane Ida, break at mid-section in very calm water? A shorter break segment from the BOP could also explain the extremely fast bending event. Now the question is how did the riser break? Subterfuge comes to mind.

  • The fact that there was no visible oil gushing out of the broken end of the riser as it sank, further confirms that the base plug at the bottom of the well had not yet breached completely (more of this in later articles) at 10:22 CDT 22 April, 2010.

  • If this was the case, why did BP, blog forums and the coast guards repeatedly stressed that “oil from the reservoir was freely flowing into the rig through the riser and feeding the intense fire on the burning rig”? Were they speculating or preparing the public for the anticipated massive oil spill that was planned but yet to happen? Again this shows that blowing up and burning the rig just for insurance claims were not the main objectives. BP's apologists have frequently stressed that this objective was pointless and they were right. The oil spill was their main objective and a blowout without the spill is like having dinner without the main course. It would be less than fulfilling especially after years of elaborate planning.

  • Rov inspection of the BOP and the seafloor around the well (BE) on 22 April 2010, showed no signs of gas plumes, blow holes or oil emanating from the well head. That would explain why the Bent Riser did not have any gas leaks on 22 April where most of the doctored-relooped footage were shown. Then 20 days later, BP showed the same Bent Riser with the orange-brown gas plume (at well A). If BP could turn on and off the gas leaks, why should there be a massive oil spill in the first place? Alternatively, BP switched wells. That is pretty obvious, is it not?

  • Even if the riser was still intact (despite the twists and bends), how could the “supposedly long riser string” plant itself inside a deep (at least 5m) crater without disturbing the overlying cemented drilling mud and sediment?

  • BP's schematics showed less than 4,000 ft of riser. What happened to the remaining 1,000 ft? Further the 700odd ft segment from well A to well BE (crater) has a totally different degree of twisting and bends from the next 3,000 ft segment. A falling elongated but uniform body like the riser does not twist and bend midway in calm water. The bottom section had to break away first and the hanging riser dropped almost vertically under its own weight as depicted in the diagrammatic illustration of BP's deepwater horizon blowout published on 30 July 2010. Consequently, the “speared location” would be centred near to its original base (or well). This again point to the location of the third well (BE) which was fraudulently depicted as leak(2) on a fallen riser. With so many irrefutable evidence, leak(2) cannot be just a secondary leak on the riser but the broken well itself.

  • There are many more flaws in BP’s official story but we shall reserve them for the coming articles. But how could entire teams of federal regulators and investigators, all failed to recognize and investigate into the flaws of BP’s official version of the disaster? Willful Blindness and Complicity come to mind. 

    You can fool all the people some of the time, and some of the people all the time, but you cannot fool all the people all the time. ~ Abraham Lincoln

    back to section 1

    (http://bklim.newsvine.com/_news/2012/02/10/10376634-bps-deception-in-the-gulf-part-1-the-farcical-3-leaks-on-the-broken-riser-story)

  • Story Photo
    • BK Lim et al (first drafted in June 2010, revised 29 Jan 2012)

    To keep this article short, we posted these figures earlier at the following links:

    Figure 165-3 BP doctored relooped video to make-believe BOP was still intact at 3rd well after 2nd blowout

    Figure 165-4 BP's latest PR twist: DWH blowout disaster downgraded into an underwater pipeline burst

    Figure 165-5 Undoctored videos confirm oil gushing blown crater was well#3 and not 2nd leak on the riser

    Figure 165-5a Doctored videos of the same blown crater confirm elaborate deception

    Figure 165-6 Even DNV was fooled by the fake relooped videos after the 22 April explosion.

    (figures 165-0, 165-1b and 165-2 are given in the next posting)

    Of all the lies that came out of the Gulf disaster, the most preposterous has been the 3 leaks on the riser story. Figure 165-0a to 165-0c were the first few schematic illustrations of BP’s blowout incident. They were so embarrassingly stupid and logic defying, most experts believed the schematics were deliberately drawn by cartoonists to confuse the average Joe Public. The patchwork of realities resembled a makeshift car hastily assembled from parts of different size vehicles. Obviously a mini car body does not match the oversize truck tires. It is obvious the 5½ inch drill pipe at leak(3) cannot be the same 21inch diameter riser (actually a well casing) at leak(2). Yet the world's technical experts willfully overlooked this fundamental discrepancy and allowed the criminals to get away with murders. And America, the world's greatest nation shouting human rights abuses all over the world, allowed this hideous crime of mass destruction in its own backyard to go unpunished? In China, the corporate criminals responsible for this environmental carnage would have been executed instead of having their lives back. Can the 11 dead crewmen, their young families and thousands of Gulf victims who suffered numerous medical problems from the toxic contaminated Gulf waters and corexit sprayed on them, ever have their lives back?

    Surely the world's most technologically advanced country could not have been so easily fooled by this “3 wells & 3 leaks on a single riser” fairy tale (concocted Beyond Phantasm). Besides the many controversial circumstances surrounding the sinking of the burning rig (DWH) and the sudden breaking of the super-strong riser in calm water, how could a third open-ended leak (3) be even possible beyond the completely severed riser at the second leak (2)? See fig165-0c. Leak(2) has to be the blown crater of well no.#3 as illustrated in many of our previous articles and irrefutably shown in Figure 165-5 with the right coordinates in the few undoctored videos.

    When you have eliminated the impossible, whatever remains, however improbable, must be the truth.” S Homes.

    Since June 2010, we have illustrated many physics of impossibilities concocted by BP. Two years later, it seems the world has not awaken from its ignorantly blissful slumber. This disaster is more than just a disastrous mega oil spill. If the world's foremost scientists and investigators cannot figure out the many fundamental flaws in the simple “3 leaks-3 wells” fairy tale, how can there be any hope of ever solving problems beyond kindergarten level? Forget the carbon tax, the ban on hazardous gas emission and just about any anti-pollution measures designed to improve the global environment. All these schemes have sinister undertones with profiting on mass miseries of others.

    In the Gulf disaster, you have the biggest environmental polluter in human history. The punishment for a crime of mass destruction that could have been averted, was just a slap on the wrist? If this is not the clearest proof of corruption at the highest level and biggest HSE (health, safety & environment) farce, then what is?

    It is clear the current political leaders had not been up to mark in dealing with this disaster. If their blinkered leadership cannot see beyond the deception in the Gulf, the only place they are are capable of leading to, is Hell. Do the American people really want to be sheepishly led down this road to hell? And world leaders follows obediently in tow.

    If we do not wake up and smell the Corexit now, pretty soon there would not be a planet to save at all.

    It was not the failure of safety regulations but the enforcement of regulations. The government admitted this much by sacking MMS's director and changing it to BOEMRE. It was not the failure of technology but the devious use of technology to cloak unfair business practices or safety farce at the very least. But would shrewd corporate criminals risk billions of investment dollars just to skimp on some daily operation expenses and safety devices? Just like the fairy tale of the 3 leaks, this was just the red herring. The oil industry will start on its decline just as the coal industry did, after its replacement by alternative cheaper and cleaner energy sources (The Future of Free Energy).

     

    Giant global oil corporations may not have the next 10 years to recover their mega billion dollar investments. With the writings on the wall and their failures to control (prevent) the advent of free energy, the oil oligarchs had to devise emergency exit schemes before oil independence becomes public knowledge. High crude oil prices cannot be manipulated too high or long enough to recoup their billions of investment dollars globally. They risk becoming economic dinosaurs.

    High oil prices depress global economic growth and hence non-sustainable for too long a period. Shallow, low cost production reservoirs are either not under their control or their reserves have already dwindled. The Middle East wars and conflicts are all about the control of cheap oil supplies. At low crude oil prices, they cannot recoup their high investment costs. Huge deep water oil reserves are just market hype. They are just too uneconomical for exploitation. But like the fake 134 billion US dollar bonds and 26 trillion US loans given out by the FED, mega oil spills could be leveraged as MIHOP environmental disasters for quick mega windfalls. More details in later articles.

    Figures 165-0 to 165-6 accurately depict how deep down the abyss the oil industry had sank into. How can we pretend that all is well with the oil industry? The 11 crewmen died not because they did not perform their job well. On the contrary, these men plus the previous drilling crew performed exceptionally well. Otherwise they could not have drilled through hell to reach the reservoir at 18,360 ft below sea level. They were on a “suicide mission” without being told that the nightmare well was supposed to blow once they had successfully reached the reservoir. It is time to put the records straight. As Edmund Burke said; “All that is needed for evil to succeed is that decent human beings do nothing”.

    The illustration of the 3 infamous leaks on a badly twisted riser, was designed to confuse and to twist public opinion to their advantage. Many experts in the industry wondered at the ludicrous illustration but no one dare to criticize big brother, BP. Below is one muffled, discussion from an astonished experienced driller at Drilling Ahead.

     

    Riser Problems?(http://www.drillingahead.com/forum/topics/transocean deepwater horizon 1#ixzz1k7tHXgvt)

    According to the Coast Guard and BP, oil is leaking from two spots along what is left of the riser system. Here's a schematic view: (figure 165-0b) dated 26 April 2010.

    Originally, the risers (represented by the blue line in the graphic above) were affixed to the blowout preventer on the seafloor, and extended 5,000 feet straight up to the "moon pool" of the Deepwater Horizon. When the drilling vessel sank, it took the riser piping and bent it around like a pretzel.

    The remnants of the riser system now follow a circuitous underwater route. According to BP, the risers extend from the wellhead up through the water column to about 1,500 feet above the seabed. Then the riser system buckles back down toward the seafloor. (Frankly, I'm astonished that it all held together as well as it has. It's a credit to the manufacturer, which I'll discuss below.)

    According to the Transocean website, the riser devices on the Deepwater Horizon were manufactured by VetcoGray, a division of General Electric Oil & Gas. The specific designation is a "HMF Class H, 21 inch outside diameter riser; 90 foot long joints with Choke & Kill, and booster and hydraulic supply lines."

    ~~~~end of quote~~~

    Why the pathetic 3 leaks on the broken riser excuse?

    If there were really 3 leaks on a single riser, BP could have easily reduced three into one controllable leak at the source by cutting the riser at the top of the blowout preventer (BOP). That was precisely what BP did at the end of May to install the LMRP (Lower Marine Riser Package) cap on 3 June 2010. But why wait for 40 days? Why would BP need to go through the charade of top kill, junk shots, hot hats and all that nonsense? Why wait for 87 days before shutting down the flow at well A on 15 July? Why was there no massive oil spill or gas leaks before 2200z (1700 CDT) 22 April 2010? See the pattern yet?

    BP's frauds and deception in the Gulf would have been exposed at the break of the disaster if they had not been so well coordinated and meticulously planned months beforehand. Official coverups could not have withstood the tsunami-force of massive public protests, even with forceful suppression. The pen is mightier than the sword. Deception is more effective in dissipating the focused energy of the masses. Once divided and confused with distorted truths, only can military force be effective in suppressing the sheepish masses to be culled. TPTB have been having lots of target practices in the third world countries and now it is time to use these tactics in their home crowd. Nothing happens by accident. Certainly not the BP's Gulf disaster which had been planned as early as 2007.

    The ROV inspections of the wellhead, marine riser and BOP in the immediate aftermath of the incident show that the mega oil spill could have been easily averted with several run-of-the-mill options. It was the sort of controllable rig blowout-fire situation the industry expects and routinely trained for. It could have been recovered safely without ending in a disastrous mega oil spill. James Cameron of the Titanic fame was quoted as saying “US shouldn't be relying on BP's underwater intel. Those morons don't know what they're doing!”. Really? Or was ingenuity behind the cloak of stupidity.

    The main reason for the deliberate blunders and delays in the recovery of the blowout and the oil spill, was to intentionally flood the Gulf with massive oil to cause market panic. No massive oil spill means no justification for spraying unprecedented massive amount of COREXIT. Bio-remediation was available and ready to be used. Yet millions of gallons of corexit had been stockpiled weeks before the mega spill occurred and surprisingly on standby to disperse on the first day itself. Yet there are those who still believe there was no vested business connection. The concerted media, political and industry deception onslaught was unmistakably deafening. Stupidity and global domination do not go hand in hand.

    The initial gas blowout (20 April 2010) which killed 11 drilling crew on the burning Deepwater Horizon rig, failed to unleash the massive oil spill as PLANNED. A detonated explosion within the well shortly after 2200z (1700 CDT) did. That triggered explosion induced a bottom hole blowout that unleashed the full power of the gushing oil from the Macondo reservoir. Period!

    Is it not a federal offense to lie so blatantly to the US Congress and American Public? Or is the system so screwed up, it is fashionable or even brilliant to get away with submitting doctored ROV videos to Congress? For the uninitiated, there were many accounts of BP committing perjury before and after Tony Hayward' congressional testimony. All ROV videos showing the still standing BOP with the Bent Riser (without the gas leak) from the 23 April till mid May 2010, were relooped footage recorded prior to the 22 April explosion shortly after 1700 CDT. Why? Because the BOP was already in pieces scattered over the seafloor after the 22 April bottom-well blowout. Again the doctored videos were deliberately ignored by investigators and mainstream media. Obvious, is it not?

    Continue: Part 1 The farcical 3 leaks on the broken riser story

  • Story Photo

    James Cameron: US shouldn't be relying on BP's underwater intel

    Those morons don't know what they're doing!
  • (Reuters) - BP Plc won a court order keeping several potentially damaging emails out of a scheduled trial to determine responsibility for the 2010 Gulf of Mexico oil spill.

    Wednesday's ruling by U.S. Magistrate Judge Sally Shushan in New Orleans came a day after U.S. District Judge Carl Barbier rejected the oil company's effort to keep evidence about settlements it had already reached out of the trial.

    The rulings came as Barbier prepares to preside on February 27 over a non-jury trial to assign blame for the April 20, 2010 explosion of the Deepwater Horizon rig, which killed 11 people and caused the largest offshore oil spill in U.S. history.

    Plaintiffs include individuals and businesses, represented by a plaintiffs' steering committee that had sought to introduce the email evidence, as well as states and the U.S. government.

    The main corporate defendants include BP, rig owner Transocean Ltd and Halliburton Co, which provided cementing services for the Macondo oil well. Anadarko Petroleum Corp, one of BP's partners in the well, is also involved in the trial.

    Shushan granted BP's request to exclude as hearsay several 2009 emails among Anadarko employees about tropical storm damage to another Transocean rig that had been under contract to BP.

    In one email, an Anadarko employee expressed disappointment that BP had not disclosed some information related to the damage, prompting another to respond: "Bummer. I'm amazed that they did not tell us about this."

    Shushan also granted BP's and Transocean's request to keep out a June 2010 email from Halliburton employee Ryan Haire questioning their reported findings regarding some tests, saying he had no personal knowledge of those findings.

    The judge also granted Halliburton's request to exclude an email from a BP geologist to a colleague in February 2010, offering "thanks for the @!$%#ty cement job."

    Halliburton contended that the email was no more than a casual, tasteless joke made by one friend to another. Shushan concluded that there was no showing that the email was a "business record" of the cement work that could be introduced into evidence.

    Barbier had on Tuesday ruled in Halliburton's favor on whether evidence of BP's settlements with Anadarko and other companies was admissible at trial.

    Halliburton had said such evidence could show the settling companies' potential bias in BP's favor, while BP had countered that they were irrelevant to establishing liability.

  • Story Photo

    Here in America, as a foreign entity you can kill 11 men, injure 17 more, cause unprecedented ecological and economical destruction to 4 states, destroy hundreds of thousands of animals, take over the media, science and regional healthcare, decimate cultures, chemically poison thousands of people, and leave a big fat mess behind, for the same cost as one bank’s government bail out, (Wells Fargo 2009).

    Heck, last year alone BP slammed a net profit of $25.7 billion. So much for the 2010 worry that BP might go into bankruptcy over the fiasco.

    And according to a UPI.com article, found here

    http://www.upi.com/Top_News/US/2012/02/05/Settlement-possible-in-BP-oil-spill-case/UPI-61971328459069/, state officials may actually be encouraging the idea, with the help of the DOJ and the administration.

  • Story Photo

    It's official: 2011 was a record-busting year in the oil industry, with the five largest companies -- BP, ExxonMobil, Chevron, ConocoPhillips, and Royal Dutch Shell -- reporting all-time-high profits of $137 billion. That's a 75 percent jump from the year before, even though the giants produced less oil than in 2010.

    It's the multinational way to go in a slumping economy: Get paid more for doing less.

  • Story Photo

    BP an­nounced today that its 2011 profit to­taled $26 bil­lion, a 114 per­cent jump from the year be­fore, when the com­pany’s “fail­ure of su­per­vi­sion and ac­count­abil­ity” caused the worst oil spill in U.S. his­tory. As the com­pany pre­pares for its up­com­ing crim­i­nal trial, let’s take a look at how BP has made out after the Deep­wa­ter Hori­zon dis­as­ter:

  • Story Photo

    Look at this important ROV video. It is a technique taken from the "Art of Mass Deception".

    How do you hide evidence by showing it?  

    Clue: Throughout the week we have been showing evidence of heading and orientation. When confused, try looking from a different perspective.  

  • On the day the Deepwater Horizon sank, BP officials warned in an internal memo that if the well was not protected by the blow-out preventer at the drill site, crude oil could burst into the Gulf of Mexico at a rate of 3.4 million gallons a day, an amount a million gallons higher than what the government later believed spilled daily from the site.

    The email conversation, which BP agreed to release Friday as part of federal court proceedings, suggests BP managers recognized the potential of the disaster in its early hours, and company officials sought to make sure that the model-developed information wasn't shared with outsiders. The emails also suggest BP was having heated discussions with Coast Guard officials over the potential of the oil spill.

  • Story Photo

    America is in trouble. This a planned disaster no doubt. We are looking at the greatest catastrophe to hit Mankind. ....And they can't fix it or won't fix it. 

    How do you bring the world's greatest Republic to its kness?

    Kindra: Does that make my people expendable?

     

  • Story Photo

    Santa Barbara cinematographer Mike deGruy died in a fiery helicopter crash Friday in New South Wales, Australia.

    According to KEYT, deGruy, 60, was in Australia to scout locations for an upcoming documentary project.

    The Age newspaper in Melbourne reported that deGruy and the helicopter’s pilot, fellow filmmaker Andrew Wight, were killed when their aircraft crashed and burst into flames during takeoff near Nowra on the south coast of New South Wales. Local authorities said both men died at the scene.

    The cause of the crash is under investigation.

    One of the films on which he worked was Deepwater Rising, which chronicled the aftermath of the 2010 Deepwater Horizon oil spill in the Gulf of Mexico. Friend and fellow Santa Barbaran Harry Rabin, CEO of On the Wave Productions and the documentary’s cinematographer, spent two months on location with him for the project.

  • It appears high-level BP officials made a concerted effort to keep secret a completely legitimate spill estimate – based on a tested scientific model – and disclosed a completely unfounded, grossly inaccurate flow rate. Go figure.

    The series of decisions surrounding the “false estimate” episode are all neatly packaged in a damning email exchange between BP employees released in federal court in New Orleans on Friday (Jan. 27). The startling new evidence provides a glimpse inside what is shaping up to rank among the biggest, most flagrant corporate coverups in recent history. From a Jan. 27 Times-Picayune report:

    The April 22 email from Rob Marshall, BP’s subsea manager for the Gulf of Mexico, to deepwater project manager Gary Imm and corporate vice president Jonathan Sprague is an exhibit in the massive oil spill litigation slated for trial Feb. 27.

    Marshall advised Imm and Sprague that an expert named Alistair Johnston had a new model for how much oil might be spewing from the wellhead a mile below the surface and 50 miles from the Mississippi River delta. Johnston’s new estimate, Marshall wrote, was 82,000 barrels a day if the well has an open hole.

    The response from Imm suggests that BP and the Coast Guard were already butting heads over how much oil was coming out of the busted well – and that 82,000 barrels a day wasn’t a number BP wanted anyone to hear.

    “A number of people have been looking at this and we already have had difficult discussions with the USCG (Coast Guard) on the numbers,” Imm wrote back to Marshall and Sprague. “Please tell Alistair not to communicate to anyone on this.”

    So much for the “complete transparency” and cooperation BP pledged to embrace.

  • In 2005 President Bush signed the Energy Policy Act, which retained the focus of Cheney's report, into law. It included what has become known as "the Halliburton loophole," which removed authority from the Environmental Protection Agency to regulate a potentially dangerous gas-drilling process invented by Halliburton.  

    These links, the fact that Cheney's former campaign press secretary Ann Womack-Colton has recently become BP's head of U.S. media relations, and the general pro-oil, anti-regulation atmosphere in the Bush years have not escaped the attention of the pundits. MSNBC's Chris Matthews highlighted the Halliburton-Cheney connection in an interview with Jay Leno on the BP spill. Frank Rich, in The New York Times, pointed out that the Interior Department degenerated into a "cesspool of corruption," under Bush and Cheney, and that the pair bequeathed Obama "a Minerals Management Service as broken as the Bush-Cheney FEMA exposed by Katrina."

  • Story Photo
    • BK Lim et al (first drafted in June 2010, revised 29 Jan 2012)

    Why would BP spend more than 100 millions USD on PR media blitzkrieg to change public perception of the massive oil spill? Remember the famous doctored photos which BP admitted to?

    http://gizmodo.com/5592836/bp-photoshops-another-official-image-again-terribly

    http://www.guardian.co.uk/media/pda/2010/jul/23/bp-oil-spill-pictures

    http://www.telegraph.co.uk/earth/energy/oil/7904221/BP-admits-it-Photoshopped-official-images-as-oil-spill-cut-and-paste-row-escalates.html

    2010 July 30- why-is-bps-macondo-blowout-so-disastrous-beyond-patch-up

    4 What you don’t see can be covered up.

    Perhaps the botched-up “photochop-chop” photos put up by BP was just a test. To see how keen the public eyes were in following BP’s clean up efforts. It would be hard to believe BP paid professionals for such a shoddy job. We should give BP more credit than that (remember the shares issues)? Let’s play dumb and the problems will go away.

    Many experts in the oil industry were surprised and questioned the rationality of capping the well when the relief wells were so close to achieving their “bottom kill” objectives. They could have installed the TOP CAP much earlier. This means that BP knew if the gushing well was completely shut at the top, the oil and gas would spread beneath the sea floor and gas seeps would start appearing. So the TOP CAP had to be placed just before the relief well was ready for the “magic show”. Hurricane Bonnie spoilt the show and the delay is already showing signs of stress (gas seeps).

    This could also mean that BP was getting less and less confident that the relief wells would work. The relief wells were held up as the last Trump card. If it fails in full (ROV) view of the concerned public throughout the world, BP’s shares would drop like a stone. There are good geological reasons why the chances of the relief wells’ success are less than 30%. But that would be in the next posting.

    So instead “of going on a public stage with a final trump card of 30% chance of success” and risking everything BP stands for, a magic show will be set up so that what ever happens, it will be a success. How?

    With a gushing well in full view, a successful bottom kill would show oil slowing down to eventually a tickle. With the cap on, it would be easier to manipulate the data. Thus botched-up photos were a test to check the keenness of the public eye. If the bottom kill fails, there is no independent monitor to prove it. BP could quickly pack and leave the site. Without ROVs’ video, the world is blind. Independent scientific researches later on could be disputed or controlled in post-recovery mopped up battle plan.

    The TOP CAP had to be installed and the integrity pressure tests used as an excuse to completely shut down the flow. There is no need to prove the well is leaking. It is already a fact. David Copperfield could not have performed better.

    ~~~end of quote ~~~~

    A primer on QC analyses of doctored ROV videos. What? BP doctored ROV videos?

    It is almost unbelievable that a respectable global giant like BP could be so unethical. If you can't make it, fake it. That was what BP did. So far we have been proven right. There is a lot more. Each time we dig, we found more dirt. Many had also wondered how we could tell the difference especially in the light of so many doctored videos released by BP. And why isn't the mainstream media keeping so quiet on BP's data frauds.

     

    With some fundamentals, you can also be your own detective. Here is the how.

    Time & space, cannot be created or subtracted but flow continuously in unison. For example, if an ROV moves from point A to B and then to C, its movement can be described by time, motion, speed and position. You cannot substitute C by A without screwing up the consistency of the all the time-spatial relationships. BP substituted well A coordinates on videos which had been recorded previously at the 3rd well location showing the BOP and Bent Riser. You might wonder why? Such elaborate deceptions played in frontal view of world's audience cannot be just for an April Fool's joke. See later articles coming up on the series.

     

    Essentially it means that you can lie to some people some of the time but you cannot lie to all the people all of the time.

    As you add more factors or constrains, the narrow path of lying becomes even narrower. It is like broadening the stage prop. Remember in the Art of Mass Deception, the stage prop is meant only for the front view audience. Look beyond the stage prop and you will see the flaws. The depth variation constrain was added to our analyses which apparently the fraudsters (not being surveyors) were largely ignorant of.

     

    All of the video footage handed to us have their time-spatial details embedded in them. Adulterating them (by us) would leave graphic evidence no matter how professionally done, especially with videos. Our job here was to prove inconsistencies and adulteration of time-spatial details. We do not adulterate videos submitted to us for analyses in order to fit our analyses. There are many ways to check this but this is not included in our primer here for obvious reasons.

     

    BP's raw video feeds were recorded independently without embedding the time-spatial details. Hence it would have been very easy for BP's technicians to broadcast even live video feeds with superficially generated time-spatial details. This is what we suspected they did generally but not all the time. Each video in question has to be examined on case to case basis.

     

    Depending on operators, the date format can sometimes switch from American (mm dd yy) to British (dd mm yy) and feet to metric. The coordinates are all in feet, but depth and altitude can be in feet or metres. The depth here refers to the ROV Depth or the height of the water column above the ROV (measured by a depth pressure sensor which had to be correctly calibrated). If there is a bulk error (say 30ft) it should rightly appear in all depths displayed. Thus, by subtracting the bulk (or datum error) we can retrieve back the right depth. Altitude, depth, coordinates, heading, are all designed for automatic input from the sensors without human intervention once the system is calibrated, up and running. Any human intervention thereafter is likely to be for fraudulent purposes other than normal operation.

     

    The water depth at the ROV location is the sum of the altitude (measured by an ultrasonic transducer to the seabed) and the ROV depth. This is where the bathymetric chart (in BP's exploration plan) comes in handy. Both well A and B have the same water depth at 4992 ft (+/- 5 ft). The third well being up slope, has a water depth of about 4960 ft. An error range of 5 -10 ft is acceptable but the sensitivity (or variation) when the ROV is stationary should not be more than 1 ft. Heading (Hdg) is the direction of the ROV, measured by the gyro, in degrees from 0 to 360. Be aware that the ROV cameras have both zoom and tilt capability. Some of the ROVs (we are told) have hind cameras mounted on them as well. Still that does not explain the motion and orientation discrepancies in the video; resulting in obvious disconnect between the motion in the video and relative position of the recording ROV.

     

    What we have been unable to demonstrate on still snaphots are the inconsistencies in the motion, speed, direction or orientation so obvious in the playback of these doctored videos? For example on a stationary viewport showing the spewing well, the recording ROV could not have move by hundreds of feet without affecting the area of view. With a stationary ROV (coordinates variation < 1 feet) the object in view (within the viewport) should move in opposite direction to the camera's rotation. For example, if the ROV is rotating to the starboard (increasing heading degrees, to the right facing the bow) the object in view should move towards the left and out of the viewport. But in BP's doctored videos, you will see the disconnect caused by superficially adding the navigation information after the field recording.

     

    One BP schill commented that BP might have accidentally merged the wrong navigation information from other dives. Perhaps. But why do these “wrong navigation information” consistently get merged for only certain sensitive locations and events? Consistency in the “accidental errors” could only mean intent to cheat under the guise of “naturally occurring” accidents or errors.

     

    In many doctored videos, you will see the heading change significantly but the BOP remained stationary within the viewport. You can demonstrate this by using a narrow beam pen-torch light shinning on an object. Of course there are the classic time skips (forward and backwards in time), coordinates jumps of more than hundreds of feets etc etc. Hopefully you can have some fun watching these ROV videos with the right perspective.

     

    BP could only fool the world because the world allows BP to.

     

    Having established some fundamentals, we now analyse figure 165-5, an early video example where the actual ground details were recorded, unadulterated. (So far we had not found any on these sets of videos but readers are welcome to feed us back if we had missed out on any). As a comparison to doctored videos, see Figure 165-5a Recycled Data, Frauds & BP's Gulf Disaster.

     

    All the 3 snapshots extracted from different videos show the famous blowout crater with the huge black oil plume, gushing out to the south (see red arrow in the RT video, bottom left). BP misled the world in claiming that this was just a leak on the broken riser. It was not. It was the blown crater of the third well, which they labeled as well BE. Why would they label the well that blew on 20 April 2010 as well BE and not well A? There is a lot more in depth details in figure 165-5. This is just the tip of the iceberg (frauds in the industry). See later articles for more amazing deception by BP.

     

    We can be quite confident on the direction of the oil flow (from the north) as the picture frame is almost parallel to the pipe (casing). The video snapshot on the lower left was captured from RT broadcast dated on 30 May 2010. The top snapshots were extracted from video recorded on 23 April and 5May(blurred?) 2010. All 3 snapshots show the supposedly 2nd leak on the riser in a crater, referred to as Leak(2).

     

    Based on our past analyses and cross-references, we beg to differ. We had argued from different angles, that leak(2) was in fact the blown crater of the third well (BE) which they intentionally blew shortly after 1700 CDT (2220z) on 22 April. Besides trying to misrepresent the third well (BE) as well A, this “missing massive explosive event” was one of the main reason BP's official story was so ludicrously inconsistent.

     

    The main story (BP's Deception in the Gulf, exposed) will explain further but for now we want to demonstrate the consistencies in the un-doctored videos on an obviously same oil-spewing crater.

     

    The graph on the right bottom is a to-scale plot of the location of the 3 wells. The red text gives the details of the ROV position as per the coordinates in the snapshot. On this video, the ROV was 43ft west of the well BE crater. Thus the heading of 97 deg is about right. The water depth (4957.7 + 4.7) of 4962 ft is much closer to the depth of well BE than well A or well B.

     

    Both the top photos show the yellow pipe (casing) to be dipping northward into the “cemented sediment” with the oil plume gushing out south. Thus all the 3 photos are consistent with each other. The fact that no coordinates were displayed for the videos on 23 April 2010, strongly suggest that BP was well aware of the sensitivity of that information. On some of the earlier videos, the coordinates were displayed as blanks or zeros. In later videos, the coordinates were falsified.

     

    What is the chance of a falling 5000ft long super strong riser (with a 3.5 million pound load-carrying capacity) breaking into two at exactly the same location the DWH burning rig was reported to have drifted to? And where is the other half of the broken riser in the crater? It could not have floated away if it was heavy enough to dig itself into more than 5m of cemented seafloor. The probability must be astronomical, considering that BP made the report (that the burning DWH rig had drifted 714 ft NW from well A) at 220402z (23:02 CDT 21 April); less than 2 days after the discovery of the blown crater. How did BP know beforehand the 5000ft riser was going to break at that point? More amazingly, could a burning rig drift in a dead calm sea, as evident from independently taken photos? BP acknowledged the semi-sub was “anchored” in place by the riser attached to the BOP at the wellhead. Is this not inconsistent with the Drift Theory? How come none of the fire fighting vessels noticed the drift at sea? Why did the reported drift came from BP's Command Centre and not from the coastguards in the field?

     

    As there is negligible slack in the non-stretchable riser, the burning rig had to sink by at least 50ft for it to move that distance. The burning DWH was observed to be listing from the morning of 22 April with the riser still intact. The DWH did not start to sink until the riser was (intentionally) severed at or around 10:22 CDT 22 April. Such precise timing!

     

    This was what we wrote on 25 Aug 2010.

    Twisted tale of the missing 3rd well that blew on 20 April 2010.

    DWH never moved 714ft NE as reported by BP to the Coast Guard. BP had to come up with something to explain why the burning DWH was in that location. The sea was calm and DWH had no power to move. This further confirmed DWH was sitting on top of the S20BC location as correctly predicted by the seabed debris forensic analysis. BP had to move the fallen BOP and placed it on Well A in the aftermath of the blowout. This is one of the many reasons BP cannot release the video footage of the BOP immediately after the second explosion blew off the BOP and broke off the bottom fifth of the riser string as detailed in The-mystery-of-the-april-20-blowout-revealed and in The-art-of-mass-deception-part-1.

    While many missing parts to the giant jigsaw puzzle have yet to be put in place, it is evident we are getting very close to the truth. Hence the intensified attacks and cointelpro on us. We had been confident enough since July 2010 to boldly publish what insiders can only whisper in private.

    The significance of figure 165-5.

    It confirms that the crater with the massive oil plume which BP claimed to be the second leak on the riser was indeed the blown 3rd well. The unadulterated videos are “consistently” consistent with our earlier assertions that the 3rd well that blew its top (BOP, well casing etc) and ended up as an open crater, gushing massive oil directly from the Macondo Reservoir 18,360 ft below. It is time the American public, victims and the world know the truth. BP had pulled wools over America's eyes with the fabricated 1 well - 3 leaks on the riser story long enough.

    You have to wonder why BP spent more than 100 million USD to mercilessly pound their fabricated lies into the mainstream media and cyberspace to conceal the truth. The massive oil spill in the Gulf is only one of their Planned-To-Happen series of disasters. It is not for fun. These disasters including 911 were planned and triggered to serve their multiple global agenda of controlling the world. The late Matts Simmons sacrificed his life to bring the American public the truth of the BP's Gulf Disaster. His death and scores of those fallen heroes, must not be in vain. We will continue to suffer as victims (one way or another) of past and yet to materialise Inside-Job disasters.

    God help us all if the truth continues to be suppressed. The next disaster may be much worse than just a massive oil spill.

    A sneak preview of the startling truths in the Gulf disaster in the coming articles.

    The making of BP’s Mega Oil Spill in the Gulf

    There was no mega oil spill before 1700 CDT 22 April. The mega oil spill could have been averted with several run of the mill options. The 20 April incident was the sort of controllable rig-blowout fire situation the industry expects and routinely trained for. It could have been recovered safely without ending in a disastrous mega oil spill. The facts will show that an explosion within the well was purposely detonated on the evening of 22 April 2010 to induce a second blowout that unleashed the high pressure oil gush from the Macondo reservoir. The second bottom-hole blowout, breaking of the marine riser and sinking of the Deepwater Horizon (DWH), were clear subterfuge from within. How could the official investigations into the causes of this environmental disaster, miss out on all these?

    The initial gas blowout (20 April 2010) which killed 11 drilling crew on the burning Deepwater Horizon rig, did not unleash the massive oil spill as BP and the government regulators had wanted us to believe. A detonated explosion within the well on the evening of 22 April, shortly after 2200z (1700 CDT) did.

    BP’s Killing Spree in the GOM

    Irrefutable proofs and connections of the dots would be presented in the later parts of this series dubbed “BP’s Killing Spree in the GOM”. The articles would show that BP knowingly drilled into 3 hazardous (high risk) well locations (not 1 well as BP officially declared before the US Congress) without adequate risk aversion precautions.

     

    It is like having repeated unprotected sex with a confirmed HIV positive partner despite being forewarned. The evidence would also show that BP’s killing spree in the gulf, unmistakably started as early as March 2010. Pro BP apologists argued the abnormal high number of stranded cetaceans (> 60 dolphins and whales) in March 2010 (a month before the blowout in April) was proof that the cetaceans were stranded from unknown natural causes before the mega oil spill. The March average for the years 2002-2009, was less than 19. They failed to mention that Methane, Hydrogen Sulfide (commonly encountered in exploration drilling), drilling mud and cement had been spilling in enormous quantities (abnormal circulation losses suffered by BP) into the gulf since February 2010.

     

    The toxicity peaked in March 2010 coinciding with the heaviest drilling losses from the 3 wells at the more problematical shallow zone; from late Feb to early April. BP abandoned well A in mid Feb with hefty drilling losses during an out of well control situation, drilled well B and well BE (3rd well) with even heavier drilling losses from 16 Mar to 7April. There is no necessity to invoke unexplained natural causes as the stranded rate correlates very well with the level of toxicity in the gulf.

    The spike for the month of March 2011 was again due to increased toxicity caused by the 9.0 Japan earthquake which shook up more oil discharges into the gulf water from the shallow oil accumulations. The statistics on the stranded dolphins accurately reflect the toxicity in the gulf water as revealed in this article,Mystery Of The New Found Oil Revealed.

     

  • NEW ORLEANS -- A federal judge has ruled that Halliburton, the Houston-based company that supplied cement for the ill-fated Macondo well that blew in the Gulf of Mexico, may not have to pay many of the pollution claims that resulted from the catastrophic spill because it was shielded in a contract with well-owner BP.

    Still, U.S. District Judge Carl Barbier said Tuesday that Halliburton is not exempt from paying punitive damages and civil penalties that arise from the April 20, 2010, blowout off the Louisiana coast. Those penalties could amount to billions of dollars.

    The judge also said Halliburton's indemnity could be voided if the company is found to have defrauded BP. He did not rule on BP's allegations that Halliburton committed fraud by declaring the cement safe to use.

  • Story Photo

    (Updated 02 Feb 2010)

    First they ignore you, then they ridicule you, then they fight you, then you win.....Mahatma Gandhi

    During times of universal deceit, telling the truth becomes a revolutionary act.......George Orwell.

    We have presented many examples of doctored ROV video with adulterated details since the start of our independent investigation on the BP's Macondo blowout and the mega oil spill in the Gulf. Although any form of adulteration is unethical, we have unearthed many forms of doctored documents, videos, survey logs and even seismic data in our QC/QA (quality control / quality assurance) work in the oil industry. Unbelievable but in reality such fraudulent practices are the norm rather than the deception. Smooth Operators work around regulations as the following extract shows.

     

    Below is a fictionalized account of the safety frauds that are occurring on a daily basis in the offshore industry.

    Nobody believes it when you are telling the truth, fictions are more believable.

    Imagine a geohazards survey vessel commissioned by an oil company (NeverDelay Oil) for an urgent survey. Geohazards surveys are always urgent and the safety clearance (insurance purposes) for drilling an oil well is always required like yesterday. But the vessel master who was contracted by the shipping agent to command the vessel just a week ago, refused to sail a vessel of such dilapidated condition.

    The vessel (let us call it M/V Broken Junk 1 aka BJ1) had been mothballed at port for many years. Although the sea worthiness and safety certificates had just been issued, the Indonesian sea captain knew better than to risk the lives of his 40 crewmen comprising nationalities from several countries including Australia, Singapore and UK, He asked for urgent critical repairs to be made first in Singapore as required by law. But the world's largest contractor (fully accredited ISO 9000 plus) also known by the name FuGold Intl (Forever UnderGoing Repairs Offshore) insisted that the vessel sail by the next 3 days. Faced with extreme pressure, the captain resigned on the spot. No problemo.

    The smooth operator always have a list of subservient free-lunch employees who they can depend on at times like this. Captain SNA (ServeAlways Noquestions Asked) answered the urgent call for duty but his medical fitness was a problem. He has been suffering from abdominal pains for months. He was afraid of going for a proper medical checkup in case his persistent medical condition grounded him permanently from offshore duties. He needed the job. This last minute call up was what he had been waiting for. He informed Fugold his medical certificate had expired (offshore workers over 50 years old require annual checkup). Again no problemo. “just fly in to port, we will arrange..” said the operation manager widely known as Mr SafetyFraud. He called up SMC (SickaPoor Medical Centre) for the instant medical certificate to be issued without physical examination. Fugold could have insisted Capt SNA take his medical examination at Manila but he would be needed to attend the Offshore Safety Survivor Safety course as required by HSE (health, safety environment) regulations. It would have taken another 3 more days. At 50,000 USD/day charge to NeverDelay Oil (NDO), it would mean a loss of 150,000 USD chargeable income, besides incurring additional berth charges at port and full onboard survey crew costs. Why bother when counterfeit safety certificates can be faxed to the vessel for cursory inspection? After all, almost all of the vessel's certificates had been fraudulently obtained in the country of registration where corruption is rampant. It would only be a cursory inspection once the credentials of the EU registered international global company is impressed upon the would-be inspectors.

     

    Fugold is accredited against the international quality standard ISO 9001:2000 and operates in accordance with a Health, Safety standard OHSAS 18001:999 and Environmental Management System standard ISO14001:2004 which is integrated with its Quality Management System. Together these systems conform to all national and international legislation as well as industry guidelines. Fugold is a member of the multi-national group of companies with 200 offices operating in over 45 countries. Clients can benefit from individual and collective experience of hundreds of survey professionals worldwide.

     

    With credentials like that, who would dare to question the authenticity of the medical certificate issued from a respectable first world country ranked as the least corrupted country in the world.

     

    The vessel sailed 3 days later after the QC Client Rep from RePeeAss (Restassured Problems Aside Intl) skimmed through all the safety papers and certificates, rushed immediately to his cabin to pass out from 3 days of booze-binge before coming offshore. Less than 3 hours out into the open sea, fire broke out at the engine room followed by a total blackout.

     

    The contractor's party chief (KendoNever SayDie) assured the crew everything was in order. He issued a warning “I am afraid we might not be able complete the survey before this old junk totally breaks down. So please rush everything just in case another fire puts us out of operation. I want everyone to keep a constant lookout for fire breakout 24/7. Our lives depend on it. We have disengaged the fire alarm. Otherwise nobody gets any sleep at all. I know it will be hot in your cabins. The chief engineer informed that the central air-con system cannot be used without risking another fire from the messy burnt internal wiring. Treat this as your privileged Sauna Bath cruise. The operation and recording rooms are fitted with new external air-con. This will be added incentives to work longer hours. Good luck and God Bless us all.”

     

    PC KNSD then ordered the engineers to by-pass the safety fuse-box with direct wiring, disengaged the pesky fire alarm and went on to report to FGHQ SF.

     

    PC KNSD: “Houston ...we have a problem....blah....blah”

    FGHQ SF: “IRY. But proceed with O survey plan, repeat urgent. Put incident as Successful Fire Drill. How's CR?”

    PC KNSD: “Still passed out”

    FGHQ SF: “Good thing we had 3 days at Manila. Put the bar tab as Mob Expenses & Port clearance. Use the Misc ER”.

    PC KNSD: “Ok, but..err..fraid' the x-wire might not hold for 3 weeks. BJ1 leaking, MER heating up, stalled a couple of times and Bilge pump NF. Other minor problems but culd burst into bigger things. Man this bucket shudn't even be out here”

     

    FGHQ SF: “Typhoon startin' in the Pacific. Shud hit landfall some time next week. Call weather, head to nearest port next week. Cebu alright? Parts heading there”

    PC KNSD: “We are too far south to be affected but Ok, Think of somethin' ”

     

    3 days later 5 am:

     

    PC KNSD: “Houston ...we have a new problem”

    FGHQ SF: “Huh? What's up? Port call another 2 days to go”

    PC KNSD: “Capt passed out. He's in extreme pain”

    FGHQ SF: “OMG. What happened?”

    PC KNSD: “His appendix burst, I think. Can't move. Can't touch stomach area. Need Medivac”

     

    FGHQ SF: “Jeezus. Finished the priority site yet?”

    PC KNSD: “No, another 5 hours to go. Err another problem.. seismic compressor gone total kaput last night. Halon gas-fire smothering system discharged by another fire in MER. Control panel burnt. No rudder control, Total radio comms blackout”

     

    FGHQ SF: “Jeezus. This is worse than I thought. Knew we shudn't hv taken that MF old junk. But GM said NO. Price as low. @!$%#. Git her for 500USD and charge NeverDelay Oil 50,000 USD/day. How much lower can u get? Log these down, will ya. Will git Mohan to give another month free for all these @!$%#in problems. Hold a minute. Get back to you”.

     

    After 10 minutes.

    FGHQ SF: “Ok. Pull up gears and head for Manila”

    PC KNSD: “What! Site not completed yet. El Nido is nearest, get there in 3 hours.”

     

    FGHQ SF: “No. Change of Plans. Reloop previous data for present site. Look Dbase in 2007 for Dummo Petroleum. They are just 50 km apart. Similar seafloor & water depth. Will pm RepeeAss on better than expected survey progress. Cite the exceptionally calm sea before the storm. Can't repair them @!$%#in French-made power supply-voltage regulator. Need to be in Manila for major rep job. Do the necessary data swap and details. Can you limp back to port?”

     

    PC KNSD: “Think so. At half speed ok but ...but Capt's in pain. Dunno if he can make it that long. Shud we drop him in El Nido first?”

     

    FGHQ SF: “No, No! Don't @!$%#in do that. Will blow our cover. No port call before Manila. It wuld be in the records. Can't have that. Open Sea okay. @!$%#! He is such a pain in the ass. Just pump in some more morphin or somethin. If he doesn't make it, report an accident or somethin that don't put us in a spot. Serve him right for getting onboard with a pre med problem. Shuld hv known better than to get him that fake MC. He will git us all into lots' trouble. Make sure it is an accident, ok? Don't ask again. Anybody knows. What about the CR?”

     

    PC KNSD: “only the mess boy and Chief mate. Can handle 'em. A big bonus'll do. At M'nila, a night out ok? Don't worry bout' CR. Gave him somethin' for his hang-over. Will keep him in bed next 2 days until M'nila. Over and out. ”

     

    (NB: Capt SNA had advanced gallstones in the bladder medical conditions. Immediate surgical procedures saved his life just in time upon landing. His doctors commented he would have died if he was brought in a bit later. )

     

    At Manila Port, 2 days later.

    NeverDelay Oil company (project manager) to FGHQ SF, PC KNSD & survey crew at sign off:

    “I want to thank everyone for an excellent job. Evrything went smoothly and exceptionally well. Best of all we beat the deadline. The CR told me you guys went overboard to save us from being hit by weather. Thanks. Let me buy you all a dinner tonight at the Hilton.”

     

    ~ above is a compressed rendition of 95% truth and 5% fiction (times, names of parties involved). With this happening everywhere in the world, it is no big surprise the videos from BP were doctored to cover the truth to conveniently play out the deception game. If things play out better than expected or the field operations run too smoothly, junk it. It never happens. Murphy's Laws always apply.

    See figure 165-5a as one of the many proofs of recycled data and doctored video. It will be apparent in the coming articles that the blown crater with the oil plume (referred to as Leak(2) on the riser) is actually the blown crater of the third well (BE). As the crater on the seafloor cannot be moving, it is obvious that BP falsified the navigation details on the video. Adulteration, faking and all sorts of frauds are being committed every day in almost every segment of the industry. Because what you don't know, don't hurt until a disaster blows up in our face. Then it is called an “Accident”. In BP's Macondo blowout and mega oil spill disaster, it was more than just an accident.

     

  • Story Photo

    Douglas H. Brown, the chief mechanic for the Deepwater Horizon, testified Wednesday that he witnessed a “skirmish” on the rig between a BP well site leader and crew members employed by Transocean, the rig’s owner, the morning of the blast.

    ¶ Mr. Brown said the disagreement followed BP’s decision to replace heavy drilling fluid with lighter saltwater before the well was sealed with a final cement plug.

    ¶ “Well, this is how it’s going to be,” the BP official said, according to Mr. Brown.

    ¶ Mr. Gowers declined to answer questions about workers’ accusations or about whether cost may have factored into the company’s decision to use the casing system it chose for the Deepwater Horizon.

  • Story Photo

    Mark Hafle, the BP drilling engineer who wrote plans for well casings and cement seals on the Deepwater Horizon's well, testified that the well had lost thousands of barrels of mud at the bottom. But he said models run onshore showed alterations to the cement program would resolve the issues, and when asked if a cement failure allowed the well to "flow" gas and oil, he wouldn't capitulate.

    Hafle said he made several changes to casing designs in the last few days before the well blew, including the addition of the two casing liners that weren't part of the original well design because of problems where the earthen sides of the well were "ballooning." He also worked with Halliburton engineers to design a plan for sealing the well casings with cement.

  • Story Photo

    Uploaded by Travinyle1 on Jun 2, 2010

    http://www.FreedomizerRadio.com
    http://www.Twitter.com/Travinyle1

    This video has not been able to play since it hit around 1,000 views

    BP Pressured Rig Worker to Hurry Before Disaster, Father Says
    http://www.businessweek.com/news/2010-05-27/bp-pressured-rig-worker-to-hurry-...
    Category:

  • Story Photo

     

    The truth of the disaster is:

    1. BP drilled 3 wells (well A, well B and then the third which was labelled BE).

    2. The blowout that occurred at 2200 CDT 20 April 2010 did not breach the base cement plug as we had analysed as far back as July 2010. It was caused by a shallow gas influx from the gas-saturated weak Sub Formation (GWSF) zone.  See http://bklim.newsvine.com/_news/2010/07/30/4781973-why-is-bps-macondo-blowout-so-disastrous-beyond-patch-up

    3. The more disastrous second bottom-hole blowout occurred on the evening of 22 April  (after 1700 CDT). It was induced by a powerful explosion detonated from within the well. This started the mega oil spill in the gulf. The BOP, riser and top hole casings were blown off the well and lay scattered on the seafloor.  In its place, the famous crater with the oil spewing out. BP called it the 2nd leak on the riser. Tony Hayward tried to twist it further by saying "It was only a small leak in a big ocean".

    4. They had to fake the standing BOP from earlier recorded footage. The only trouble is ....there was no gas/oil spewing from the cracks in the Bent Riser. Because the videos on 23 April onwards were all recorded before the 2nd bottom hole blowout. 

    5. 20 days later, they reassembled the riser onto a new BOP at well A. What you saw then was the "fake blowout gushing well" while the real gusher well was bellowing 720 ft NW of well A.

    Hard to believe. Stay tuned as we present even more evidence. If this is not the truth, we would have been tripping over a thousand times since July 2010. The fact that we did not, shows we had been on the right path towards unearthing the whole truth about this disaster. The truth is so much stranger than fiction. Wait till you read the coming series, currently in their final drafts.

    BP's deception in the Gulf, exposed.

    BP's killing spree in the Gulf ~ dealing with long term environmental consequences of the Gulf disaster

    The mafia in the global oil industry ~ the crime of mass destruction and unscrupulous market manipulation behind these mega oil spill disasters.

  • Story Photo

    Washington, DC — Top Obama officials manipulated scientific analyses of independent experts to seriously lowball the amount of oil leaking from the BP Deepwater Horizon, according to a scientific integrity complaint filed today by Public Employees for Environmental Responsibility (PEER).

    Documents obtained by PEER through a Freedom of Information Act lawsuit indicate White House pressure to present low-range estimates as best estimates. In fact, numbers presented to the public were less than half the true flow rate.

    On May 19, 2010, one month after the Deepwater Horizon catastrophe, the White House announced creation of a group of experts from academia, industry and government to generate an accurate and independent estimate of the oil leak rate. This group was called the Flow Rate Technical Group (FRTG).

    Using new scientific integrity rules, PEER today filed a complaint charging that the leader of one of the FRTG Teams, Dr. William Lehr of the National Oceanic & Atmospheric Administration (NOAA), manipulated the scientific results of the FRTG experts throughout the entire crisis to significantly understate the spill rate. Lehr is also the author of the now infamous “Oil Budget Calculator” and a report concluding 75% of the oil was gone from the Gulf by August 2010.

  • Story Photo

    The pictures speak for themselves on the gross distortion of truth. Are we going to let BP get away wit this? Did 11 crew die in a preplanned mega oil spill?  Three things you cannot hide, the SUN, the Moon and the Truth ~ Buddha.

  • Story Photo

     

    According to all mainstream media and investigation reports, the gas blowout on 2200 CDT 20 April 2010, started the oil gushing out of the Macondo Reservoir continuously for the next 87 days. Total estimated oil leaked: 5 million barrels. Yet on all the video footage on 22 April 2010, there was no leaks at all.

    Early morning of Friday, 23 April 2010, CBS News broadcast the following statement from the Federal On-Scene Coordinator Rear Admiral Mary Landry (the ranking federal official on the spill response at that time):

    “At this time there is no crude emanating from that wellhead at the ocean floor . . . . there is no oil emanating from the riser either. That statement was made after BP enlisted remotely operated vehicles (ROVs) to investigate the immediate wellhead area. Footage shown from those ROVs did not show any leaks”.

    BP’s own videos at http://OilSpillhub.org show no leakage at this time.

    Yet 20 days later, the world was mesmerized 24/7 with the live broadcast of the Gushing Well? How did BP manage to turn on and off the well? Why were the videos from 23 April 2010 till mid May showing the BOP with the Bent Riser all doctored with falsified ROV details, inconsistent coordinates and headings? This has to be the greatest magic (deception) show on earth; "BP's deception in the GUlf". 

  • Story Photo

    Tony Hayward, the former chief executive of BP, has been accused of giving untruthful evidence to US Congress, by plaintiffs suing for damages over the Gulf of Mexico oil spill.

    In court filings, lawyers argue that Mr Hayward "at best, has a unique view of the truth", citing his congressional testimony from June 2010, in which they claim he was untruthful over the scope of BP's internal investigation into the disaster.

    The allegations were made in response to BP's attempts to preclude parts of Mr Hayward's deposition - when he was questioned by the plaintiff's lawyers in preparation for the court case - from being used in evidence at the trial on the grounds he was asked "improper questions".

  • Story Photo

    Uploaded by JMacQ77 on Aug 24, 2010

    This a shortened version of the video captured on 7 July 2010 at 1:54PM by Youtube user "X2YeZCAMCNC," so thanks to him or her. This shows once again, this time with excellent video quality, the well at site B which BP says does not exist. Taken from the Skandi Neptune ROV 2 video feed.

  • Story Photo

    You will never hear this on the main news.

  • Story Photo

    An Ill-fated Discovery
    According to news accounts, at about 10 p.m. CDT last Tuesday, Deepwater Horizon was stable, holding an exact position in calm, dark seas about 45 miles south of the Louisiana coastline. Water depth in the area is 5,000 feet. The vessel manifest listed 126 souls on board.

    Deepwater Horizon was finishing work on an exploration well named Macondo, in an area called Mississippi Canyon Block 252. After weeks of drilling, the rig had pushed a bit down over 18,000 feet, into an oil-bearing zone. The Transocean and BP personnel were installing casing in the well. BP was going to seal things up, and then go off and figure out how to produce the oil -- another step entirely in the oil biz.

    The Macondo Block 252 reservoir may hold as much as 100 million barrels. That's not as large as other recent oil strikes in the Gulf, but BP management was still pleased. Success is success --
    certainly in the risky, deep-water oil environment. The front office of BP Exploration was preparing a press release to announce a "commercial" oil discovery.

  • Story Photo

    PLEASE sign the online petition:
    http://www.gopetition.com/petitions/demand-independent-survey-of-bp-s-relief-...

    The government documentation provided in this video Prove beyond any reasonable doubt that BP is lying about the status of the Relief Well D in the Gulf of Mexico that was drilled as a means to 'kill' the original Macondo well that blew. The Relief Well D was reportedly sealed by BP in September 2010. Why and how was a BOP Test ran on a 'permanently sealed' and capped well? That my friends is physically IMPOSSIBLE! So, now that you know, are you going to allow our government to continue covering up for BP and allowing them to manage their Own Crime Scene? Or are you going to be a voice of courage and reason?

    Links to publicly available documents at BOERME:

    WAR Reports
    (3-6-11) http://www.gomr.boemre.gov/homepg/fastfacts/war/war.asp?-169939
    (2-8-11) http://www.gomr.boemre.gov/homepg/fastfacts/war/war.asp?-169392
    (8-22-10) http://www.gomr.boemre.gov/homepg/fastfacts/war/war.asp?-161557

    APM's
    (8-19-10) http://www.gomr.boemre.gov/homepg/fastfacts/apm/apm.asp?-128502
    (2-8-11) http://www.gomr.boemre.gov/homepg/fastfacts/apm/apm.asp?-130805
    (3-2-11) http://www.gomr.boemre.gov/homepg/fastfacts/apm/apm.asp?-132244

    End of Ops
    (3-8-11) http://www.gomr.boemre.gov/homepg/fastfacts/EndofOperations/eor.asp?-111448
    (8-21-10) http://www.gomr.boemre.gov/homepg/fastfacts/EndofOperations/eor.asp?-111448

    Again, a sincere Thank You to Shirley Tillman, Lorie Williams, Laurel Lockamy, and Trisha James. Also Thank You Dahr Jamail reporter and Erika Blumenfeld photographer for AlJazeera and all the Gulf Warriors who are continuing to report the ongoing depth of the true devastation in the Gulf of Mexico due to BP's disasterous explosion of the Deep Water Horizon.

    This research and accompanying petition are solely the expressed opinion of Rhea Aker.

  • Story Photo

    What really brought down the deep water horizon?

    Continuing oil leaks from the reservoir & spraying of corexit are creating health problems in the Gulf.  You need to listen to this series of video, to understand the crimes BP had committed.

  • Uploaded by lockamy1 on Jan 20, 2012

    I took this video of HUNDREDS OF DEAD FISH every step on he beach KILLED BY THE BP OIL SPILL on 6-9-11 in Gulfport, Mississippi

  • Story Photo

    Today is Thursday September 29, 2011. A friend of mine just returned from Venice, Louisiana on a fact finding mission. He spent 2 days there and talked to dozens of fishermen and BP contractors and Coast Guard personnel and there is alot of oil at the Deepwater Horizon-Macondo well site. It is not a sheen, It is several inches thick in some spots. A chemical analysis has confirmed it is Macondo oil.There is alot of activity in Venice and resources are being ramped up.
    Word is that geological formation above oil deposit is unstable and oil is leaking from fissures around wellhead. All sealife on ocean bottom is dead according to Woods Hole Oceanograpic Institute in 30+ mile radius from site and Corexit dispersant is present in large amounts. According to Sergio Alex Villalobos who is a toxicologist for Nalco, the company that makes Corexit,”Once It’s mixed with oil,that’s where you get the most impact, that’s were you see most of the toxicity”.
    He was quoted in the September 2010 issue of Scientific American magazine on page 26. There are alot of sick people that worked on the initial oil spill cleanup and residents in many coastal towns and cities that are sick. This is the second inning of a long nightmare and anyone who signed a release to get a ‘quickpay’ from BP and their minion Fienberg should hire a lawyer asap and hope they can get their release annulled. BP top brass are sociopaths… “

  • Only 17 months before BP's Deepwater Horizon rig suffered a deadly blowout in the Gulf of Mexico, another BP deepwater oil platform also blew out.

    You've heard and seen much about the Gulf disaster that killed 11 BP workers. If you have not heard about the earlier blowout, it's because BP has kept the full story under wraps. Nor did BP inform Congress or US safety regulators, and BP, along with its oil industry partners, have preferred to keep it that way.

    The earlier blowout occurred in September 2008 on BP's Central Azeri platform in the Caspian Sea.

    As one memo marked "secret" puts it, "Given the explosive potential, BP was quite fortunate to have been able to evacuate everyone safely and to prevent any gas ignition." The Caspian oil platform was a spark away from exploding, but luck was with the 211 rig workers.

    It was eerily similar to the Gulf catastrophe as it involved BP's controversial "quick set" drilling cement.

  • Kimberly Wolf, a Gulf Coast resident and environmentalist affected by the BP oil disaster, was one of the featured speakers at the Spill into Washington D.C. rally on Labor Day weekend 2010. This is the first half of her speech from 9/5/10.

  • --Scientists Fear Fresh BP Oil Surfacing at Deepwater Horizon Site Is Making Landfall 100 Miles away --As public concern escalates, the critically acclaimed oil spill documentary "The Big Fix" premieres Nov. 12th-14th in Los Angeles

     

    The Gulf Coast is reeling from reports that fresh oil rising from BP's Macondo Reservoir - ground zero of last year's massive spill - is coming ashore, again. Scientists have confirmed the existence of a "second wave" of BP oil fouling Gulf waters and beaches, poisoning marine life and wildlife, and posing a grave public health risk.

    While federal officials fail to acknowledge the problem, the situation in the Gulf worsens by the day. "It's deja vu all over again, in the very worst way," says New Orleans-based environmental attorney Stuart H. Smith. "We have fresh oil surfacing again at the Deepwater Horizon site.'

    Through rigorous "fingerprint" testing, LSU chemist Ed Overton confirmed that slicks sweeping across the Macondo Prospect since mid-August are made up of BP oil. "It is a dead-ringer match," Professor Overton said. "I was amazed that the ratios matched as good as they did."

    Chemical confirmation that the oil is from the Macondo wellsite provides vindication for those who pursued the truth for months despite a hard-nosed campaign of denial, intimidation and obfuscation executed by BP and its partners in the federal government. It is this very type of corporate-government "teamwork" that The Big Fix - the critically acclaimed oil spill documentary - portrays in riveting detail.

    Based on lab-certified test results of oil samples taken last month on Horn Island - a narrow strip of federally protected land just 12 miles off the Mississippi coast -researchers believe that fresh BP oil from the Macondo Prospect has made landfall more than 100 miles north of its origin.

  • There were "many, many restrictions" within the well and other drilling equipment on the seafloor, Suttles said, dramatically slowing the release of oil. "This is a long way away from something more significant."

    Events soon proved Suttles' reassurances to be terribly misplaced. The leak rate at the time was far, far higher than BP portrayed to the Coast Guard -- more than 50,000 barrels per day from the moment the rig went down until the well was capped 87 days later, a government-led panel of physicists and engineers would conclude that August. At that rate, the leak had produced an Exxon Valdez-sized spill at least every five days.

    Today, more than a year after the spill ended, serious questions remain about BP's role in estimating the size of the undersea gusher.

    What is clear is that BP failed, throughout the event, to produce an accurate estimate of the size of the leak to the federal government or the public. Also readily apparent is the company's strong vested interest in downplaying the size of the spill: federal pollution laws stipulate fines as high as $4,300 for every barrel of oil unlawfully discharged into U.S. waters.

    Less obvious is precisely how and why the multinational energy giant fell so short in its efforts to determine the scale of the disaster. BP officials have adamantly denied deliberately lowballing the size of the spill, arguing that the company was overwhelmed by the technical challenge of measuring the deep-sea leak and claiming that the government shares equal responsibility for the early flow estimates.

    Yet a review by The Huffington Post of thousands of pages of documents, along with interviews with dozens of engineers, scientists and government officials, has uncovered new information challenging BP’s portrayal of its efforts to measure the leak -- and found the company may have withheld crucial data on the well’s flow rate from federal responders during the spill.

    According to federal officials, BP was solely responsible for producing the very first spill estimate of 1,000 barrels per day, a figure which led to a sense of complacency about the seriousness of the event among some federal and state responders at the outset of the disaster, the presidential commission on the oil spill concluded in January 2011. BP has never publicly acknowledged generating this figure and even the commission’s investigators could not determine the methodology used to produce it.

  • Water sample analysis conducted independently by EcoRigs shows a positive correlation to BP’s oil spill samples. “The presence of fresh BP MC 252 crude oil in surface waters 2 to 14 months after the well was reported to have been capped suggests that crude oil from the BP DWH MC 252 field may have found new pathways to the seafloor.” The evaluations conducted also reveal that the toxic chemical Corexit is now being applied to the subsurface leak located 1500 meters beneath the ocean’s surface at the wellhead. This is done with the intention of further decomposing the oil so that the smaller particles do not make it to the surface and the continuing oil spill can be easily kept from the public eye.

  • Story Photo

    In a 43 minute television documentary investigation supported by documents, testimonies, visual proof and first hand straight forward lies from BP, the program Conspiracy Theory hosted by former Minnesota governor Jesse Ventura pulled the curtain off the cover up and revealed that the oil spill was not only an accident, a disaster, a tragedy, but it was in fact a carefully crafted event to bring about coastal mass depopulation, death, sickness and control of resources; all on behalf of corporations. The documentary not only reveals one of the largest conspiracies I have ever learned about, but also points out how the oil spill is part of a series of test events to cause the depletion of the gulf area in order to cause the mandated migration of at least 17000 families, many of which have lived there for over 100 years. The depopulation plans are not limited to the coastal areas or the Gulf of Mexico. It extends to as far inland as Louisiana.

  • Story Photo

    A BP scientist identified a previously unreported deposit of flammable gas that could have played a role in the Gulf of Mexico oil spill, but the oil giant failed to divulge the finding to government investigators for at least a year, according to interviews and documents obtained by The Associated Press.

    While engineering experts differ on the extent to which the two-foot-wide swath of gas-bearing sands helped cause the disaster, the finding raises the specter of further legal and financial troubles for BP. It also could raise the stakes in the multibillion-dollar court battle between the companies involved.

  • Story Photo
    • by BK Lim (7 Sept 2011, revised 13 Sept 2011)

    This is one of the several inquiries from concerned residents in the gulf:

    I recently made a post to your wall regarding the NOAA vessel Okeanos Explorer which in past weeks has spent a great deal of time running grids in the Macondo Well area. If you click on the link in the message it will take take you to the NOAA Fleet Map. In the left hand column you can click on the Okeanos Explorer button and it will highlight that vessel's location, which at present shows it still in the Macondo area.

    If you click on the Okeanos symbol, which is EX, a window pops up. Within that window is a link showing the vessel's latest track. You can zoom in on that track with the tool provided in the left hand corner of the screen. After reading through the list of this vessel's capabilities, my guess would be that they are mapping the sea floor extensively in this region. They also ran down the ridge along the entire Florida coast south to the Keys.

    I was wondering if you might have any thoughts on what information they might be able to gather or what they are looking for.

    http://shiptracker.noaa.gov/gShiptracker/map.aspx

    NOAA Fleet Map ; shiptracker.noaa.gov

     

    1. Thank you Peter for alerting me on this. Had been busy with some "discoveries" on the tsunami-triggering devices. Another stealth weapon of mass-destruction with enormous economic spinoff for the perpetrators. There is always a broad spectrum of stocks you can invest in and short sell to reap enormous windfalls on an accidental "disaster" that could be reliably predicted well before hand.
    2. Since the beginning of the disaster, experts had known the wide and long term consequences of the Macondo Blowout. The perpetrators knew as well but it was to their interest to narrowly focus on just Well A; so as to avoid highly embarrassing questions for which the answers were blatantly obvious.
    3. They were at the same time also interested in knowing the scope of their destruction; in preparation for their next disaster in the pipeline.
    4. But they could not openly survey in the immediate aftermath of the blowout. It would be an open admission that the late Matts Simmons and many gulf-truth advocates were dead right. Well A was just the dud. The blown crater at the 3rd well was spewing more than 100,000 barrels per day. Even worse the highly corrosive mix of brine, and gas ingress into every crevices and permeable sections of the formation, creating new pathways to the seafloor for the heavier hydrocarbons from the Macondo reservoir.
    5. A seafloor survey then would have revealed the ugly truths about the broken seafloor and precarious salt formation they were trying so hard to hide.
    6. So why now?
    7. Well, thanks to hard working and persistent gulf-truth activists (Trisha Sprinstead, Trisha James, Real Coastal warriors, Maureen, Michele & others) and the unfortunate recurrence of dead wildlife, tainted seafood, oil slicks etc, the fundamental issues of the BP Gulf Oil disaster were kept alive. Contrary to what the court and regulators said, the number of sick gulf victims increases and the gulf water is not getting any better. BP has no choice but to come up with a better PR exercise, one that is more convincing in stamping out the persistent doubts of BP's “good intentions to make the Gulf as good as before” if not in deeds but at least in a documented “scientific research” remotely controlled and funded by BP.
    8. Is this supposed to be the “ultimate survey-research” that will put an end to more than 15 months of “speculations”? No wonder WHOI would have no part of it. If I refused as WHOI had, I could then be dismissed as being “not credible” and unwilling to submit to ground-proofing.
    9. After more than a year of grouting, patching up and destroying all critical evidence in the seabed around the Macondo wells they are confident enough, the "modified seafloor" would not be criminally incriminating. It is akin to letting a murderer a month to clean up the crime scene before sending in the CSI team. Previous ROV videos showed planted marker ropes and buoys at the known gas vents and oil seeps locations at between 50 to 700m from well A. See one video of the gas / oil vent at http://www.youtube.com/watch?v=MgDxR0nYTFo
    10. Having marked and monitored these gas / oil vents, it would be easy for BP's funded seafloor survey to avoid those locations with a single sweep lines a few tens of metres apart. The irregularly spaced lines would have too much uncovered zones in between to be of significant value.
    11. The fact that the seafloor survey (using the various multibeam sonar and sub-bottom profiling techniques) has been delayed by more than 15 months is by itself an open admission BP had a lot of skeletons to hide in this disaster. Such seafloor survey should have been conducted as soon as possible as to determine the causes of the disaster. So my strong hunch is that this belated seafloor survey is nothing more than a carefully choreographed survey designed to show the world that the Macondo Disaster had ended and the new oil spills are nothing more than natural random spills.
    12. So now you see why I was asked to submit my recommended locations for ground proofing?
    13. It was a well-calculated risk game that BP could not loose...akin to “Head BP wins, Tail BK lose”. I had played this game many times in the past. Rov camera view is like a “pin-hole” view of the universe. A gas vent or oil seep just a few metres off the ROV track and you see nothing. Without an expert's interpretation, many of you would not make anything significant out of the video shown in (9). In fact if I had not followed a rov live tour of the seabed on 1 Nov 2010, I could not have been so dead certain of the seabed conditions.
    14. see http://bklim.newsvine.com/_news/2010/10/31/5386300-a-new-drilling-rig-at-macondo-site?commentId=18975303#c18975303 ….quote “ LT, I had a 2 hours live tour of the seafloor around the site last night. It is a lot worse than we thought. Will be writing on it shortly.” …..#4.3 - Mon Nov 1, 2010 6:15 PM PDT
    15. Should I obediently followed BP's orders into the “trap”? Heck no, especially when so many of my predicted scenarios are being proven right.
    16. Should I be surprised I was asked to recommend some locations to check with the ROV, so soon after BP's denials of the new oil spills in late August 2011? How could BP be serious about finding the truth of the new oil spills if they had already outright rejected any connection to the Macondo Wells and blowout in April 2010. I do not blame my contacts and those gulf-truthers who had been working hard to get my assessment verified. BP should know better than to come up with this trick of “urgent requests” at the very last minute. I am sure they had the research-survey cruise planned months ago.
    17. There was no excuse for such a last minute request on 30th Aug 2011: “BK, I need to know what needs to be looked at and photo'd to support your letters claims that oil is leeching from the fractures and fissures justifiying the concerns addressed in your letter. Do you know the GPS coordinates and location that need to be re visited with the discovery being requested. Time is critical as BP and USCG has assets there, trying to determine where the oil is coming from.”
    18. But I was prepared. Instead of specific locations, I requested “routine systematic mapping” in which the survey lines were run on regular grid-lines with data scan overlapping and crossing each other. This is how all site surveys had been conducted. Many leading geohazards survey companies like Fugro had been caught cheating trying to beat the grid-line survey system. You can't since adulterating the data on some lines will lead to discrepancies on the other lines. It is like you can cheat on some lines some of the time but you cannot cheat on all the lines at the same time. But with single lines recce, you cannot tie in data from isolated lines. There is a lot of room for adulteration. Why waste millions of dollars on a survey that is going to be full of holes and open to serious technical contention?
    19. BP's Macondo bathymetric chart was supposedly surveyed using an AUV with MBES. In truth, the chart was compiled from a surface single beam echo sounder, a secondary backup system in the event the AUV mounted MBES (primary system) failed to function. It is an industry-wide scam because leading geohazards survey companies get away with such crimes with impunity all the time. BP's erroneous Macondo bathymetric chart is one documented example of such a scam.
    20. See http://bklim.newsvine.com/_news/2010/09/03/5039904-forensic-analysis-of-bps-bathymetric-chart
    21. Struggling between airports and travelling with a high fever, I managed to send in my recommendation of a detailed AUV (autonomous underwater vehicle) survey utilising multibeam echo sounder (MBES), seafloor mapping system using side scan sonar and sub-bottom profiling (4x4 pinger); all of which are standard site survey tools. See figures 161-1 and 2 which are self-explanatory.
    22. My survey recommendation was the minimum to establish the link between between last years oil spew (scattered rov videos with adulterated coordinates), the seafloor and sub-seabed features with the recently observed oil slicks.
    23. If we can establish where the past and recent oil had surfaced at the seabed, we can generally interpret the "migrating" and widening circles of new pathways since April 2010. This information would be critical in designing battle plans to solve the worsening periodic oil spills the Gulf is going to experience time and time again whenever there is shallow crustal adjustment. It is no coincidence the recent new spills followed the 5.8 (mag) 6km (depth) 23rd Aug 2011 shallow quake 8 km SSW from Mineral, Virginia. The last major oil slicks were observed in mid to late March, following the great (9 mag) Japan quake on 11 March 2011.
    24. Although data from the ongoing seafloor survey carried out by Okeanos Explorer since 1Sept 2011 are not yet available, the different emphasis in survey coverage is already telling.
    25. The vessel's track history seemed to suggest a higher emphasis in the south-western edges of the Biloxi Dome, the southern edged of Whiting Dome and generally south of the Macondo prospects. While there may yet be geologically valid reasons for the emphasis south of the Macondo wells, the shelf edges 6 to 8 km north-west of Macondo Wells and the badly eroded north-western edges of Whiting Dome should at least be surveyed with some grid-lines (see areas A and B in figure 161-2, 161-2A and 161-3).
    26. BP's vessels and drilling rigs had been observed working for quite some time in both areas (A & B) even after the well was supposedly capped in 15 July. The 22 mile long underwater plume (first denied by BP and later confirmed by many independent research cruises), was suspected to have originated from the cracks in the seafloor at these locations. By avoiding these critical areas, can the present survey investigation be truly objective and independent in investigating the truth of the Macondo Blowout?
    27. Almost all the oil sightings are north of the Macondo wells, not south. Why did the survey deliberately (?) avoid the shelf edges north of Macondo to concentrate in the south? In March 2011, new oil spills were suspected to have come from "leaks in the seabed" north of the Matherhorn field. The shelf edges bordering the Mississippi-Alabama Shelf, appear pretty fractured with large crevices and in potential danger of sliding into gigantic submarine landslides. Submarine landslides are more effective in generating tsunami than quakes without significant landslides. Both the 2011 Japan and 2004 Sumatra Quakes had giant tsunamis due to the accompanying large submarine mass displacement.
    28. If the Okeanos Explorer could afford to survey the shelf edge all along the West Florida Escarpment down to the Florida Keys, why can't BP or the organisers of the research-survey cruise spare some effort to survey the more "rugged" shelf edge bordering the Mississippi -Alabama Shelf where the new and past oil slicks had been observed?
    29. Is the main objective of the BP-funded and probably BP-directed research-survey cruise, to reconnaissance for naturally occurring oil/gas seeps and other geological data to substantiate and distance the new-found oil slicks from the Gulf Oil Spill disaster that originated from the Macondo Blowout on 20 April 2010? Could the main objective be looking for any evidence to absolve BP from living up to their legal obligations; rather than seeking the truth?
    30. These are my expressed concerns following numerous inquiries on the "strange" course of action taken by NOAA. NOAA can survey every inch of the Gulf seafloor for the next 30 years (for all we care) but should the priority not be determining the linkage and long term consequence of the Macondo Blowout first?

     

  • Story Photo

    Then came a horrible abscess on the side of her face, near her eye. In just hours, her face blew up like a basketball, and she was rushed to the hospital. They lanced it, gave her three antibiotics, sent a sample off to be tested.  It wasn't a staph infection.  She had to return three times before it became manageable.  Then, she developed a rash. Not an ordinary rash, but giant boil-like lesions that burst, leaving crater-like hideous scars all over her legs an' arms.  Again she is on antibiotics, but the rash still comes an' goes.

    Her test results are available to anyone who wishes to see them, an' show that she is quite toxic. Benzene, Toluene , m.p-Xylene, Hexane, 2-methlypentane, 3-methylpentane, at dangerous levels.

  • Here it is: videographic evidence of massive amounts of oil and Corexit all over the Gulf beaches, both before and after Hurricane Lee. I want to emphasize that this is happening NOW. These are not shots from 2010. If you ask me, this is pretty damning evidence that the BP Gulf spill is not cleaned up–and that oil in the Macondo Prospect could still be gushing through cracks in the sea floor. Why this is not major news is beyond me.

    Thanks go out to the photographers and videographers who captured these images. (Credits can be viewed by clicking through to YouTube.)

  • Story Photo

     

    • by BK Lim (first written in July 2010, updated 5 August, revised 10 August 2011)

    One of the most important lesson I learned from the BP Macondo blowout disaster was:

    “When the student is ready, the teacher will appear” ~ Buddha.

    In the months following the 20 April 2010 Macondo blowout, when the world in particular the residents of the Gulf was still oblivious to the crimes and frauds committed by BP; when hopes ran high that BP would have the financial resources and the Obama Administration the political will to see to it that “BP would make things right” and the “Gulf returned to its pristine condition before the disaster”, you could shout all the truth you want and it would still fall on deaf ears. In June 2010 my introduction a geoscience seminar paper was as follows:

    Prediction is inherent in Geophysics, more so in geohazards geophysics. Without predictions, geohazards surveys are nothing more than hydrographic surveys. Yet geohazards predictions are often treated with disdain if the risk of geohazards is high. Many would prefer the risk of geohazards to be downplayed in order for the project or drilling to proceed smoothly as planned. In the event of an unlikely disaster, the “safe geohazards assessment” is always handy in absolving blame and financial responsibility. It is also easy to blame massive financial losses on geohazards which like all natural disasters are acceptable “force majeure”. The chain of human errors especially the erroneous geohazards prediction and interpretation leading to the disaster is often lost in the chaotic aftermath.

    In essence, geohazards surveys serve as insurances against the risk of disaster, without which there can be no financial backing for the project concerned. But like all insurances, the insured needed to get a clean bill of health before being insured and that “health certificate” is the geohazards assessment report. Being commissioned by the insured (the Clients), it is easy to see where business loyalty lies and why the geohazards prediction failure rate is so high.

    Sixteen months after the disaster, the truth of the disaster is still covered under layers of mud (deceit) and the 6 billion citizens of this planet are still denied justice. So what is new? For generations, the masses had been lied to and any new disasters (man-made, natural or made-to-happen-on-purpose) will similarly be covered up and twisted to benefit the powers in control. Will this Gulf Oil Spill disaster or the Japan Nuclear fallout disaster be any different from past disasters the world had experienced? Will we ever learn the painful lessons? By the time we smell the COREXIT, it will be already too late. Cover ups will only lead to more disasters in the future. Do we really want more disasters?

     

    In the last six months, the oil mafia have tried every tricks in their sleeves to eliminate me from the face of this earth. By GOD's will I am still alive though there has been more than a dozen lives lost as collateral damages. Innocent lives lost or nearly lost through mistaken identity shooting / killing or just plain “in the wrong place at the wrong time”. How many of the dead corpses turning up in Singapore's reservoirs, waterways and other secluded locations were mistaken identity killing and how many were accidental eye witnesses? How do you explain the lack of eye-witnesses to the numerous murders happening in one of the most densely populated island in the world? That would be the topic for the forth coming article.

     

    As proof of the gross injustice and the lopsidedness of the investigation into BP's crimes and frauds in this Gulf disaster, see the following video footage of the BOP; the smoking gun of the disaster and tell me there was nothing fishy. Bear in mind even the simple cleaning off the logo job under 5000ft of water could cost as much as USD100,000. But why was there a need to wipe off the logo and label if it was the original BOP stack? If the logo and company label was on a replaceable section of the BOP, could they not wipe them off while it was still on deck at 1/100th of the cost?

     

    Sometimes it is the little oversights and overlooked mundane tasks that spoil the whole orchestrated BOP switch operation. There were also the “little” discrepancies here and there that did not quite fit into the symphony of deception.

     

    For example, BP reportedly started the top kill on 26 May 2010, more than 1 month after the blowout. Okay, even if BP was given the benefit of doubt in pussyfooting, it still does not explain why there was a “dangling BOP” from 3 to 16 July 2010

    when the world was mesmerized with the constantly gushing BOP stack on top of Well A from May till 15 July 2010 when the well was finally capped. BP had maintained that the BOP Stack could not be removed from the gushing well, for fear of escalating the oil spew. The damaged BOP stack was officially removed for the first time on 3 September 2010. Besides the biggest lie that BP drilled only one well, this would be the second biggest lie of the century in the oil industry.

     

    Many industry's insiders were really surprised at this daring “poker game” gambit. If the BOP had been badly damaged as asserted by BP and as evident from the disastrous blowout, it served no purpose to keep the damaged BOP in place. If the expert drilling crew could not control the blowout, it usually means the well head, well annulus and the Formation around the blown well at the near seafloor zone are broken beyond repair. The BOP being the strongest would be the last to be damaged. But even if the BOP was not damaged beyond repair, it would still be pointless to keep the BOP on the broken well head. When a wellhead is broken beyond repair, the most logical procedure to kill the well is by intercepting it at the most strategic section (with reference to the geologic formation) well below the damaged zone. Any top kill would only make a bad situation worse as I had said back in July 2010 – the high risk of capping BP's gushing well from the top.

     

    http://bklim.newsvine.com/_news/2010/07/19/4704785-the-high-risk-of-capping-bps-gushing-well-from-the-top

     

    The illogical and incomprehensible maneuvers by BP in the aftermath of the blowout, had been viewed suspiciously by industry's experts as buying time and “muddling the pool” to mask their covert operation of setting up the second (fake) BOP on an undamaged wellhead which was Well A abandoned in mid February 2010 (see “Which well are they killing?” published on 1 Sept 2010). http://bklim.newsvine.com/_news/2010/09/01/5024700-which-well-are-they-killing

     

    A novice in crime without political support and firepower would not have dared to pull such risky gamble; a technical ploy “full of holes”. Yet they did successfully in full naked view of 6 billions inhabitants of this earth. I was not entirely surprised that they went ahead with the charade. After their block buster success with 911, who could stop them?

     

    What I was surprised was the willful blindness by the “respectable” investigators on these glaring discrepancies? It was from that point onwards that I lost all faith in the Oil Industry, in governing and regulating themselves in the interest of Mother Earth. How naïve I was all these years, thinking they did not know? Of course they knew of the safety frauds and violations; the unscrupulous business deals that kill silently hundreds if not thousands.

     

    How could these “respectable and highly professionals” not see that the nakedness of the Emperor wearing nothing but BP's magical robes made of cloths woven from fine invisible golden threads? Even ordinary folks outside the industry could see and questioned the numerous ROV sightings of BOP at well B or close to it, at the third well location (S20BC) and several other locations in various poses. Shame on the so-called veteran experts at TOD for putting down those who questioned these ROV sightings. I reckon it is the duty of every oil company man to cover up for their company's mistakes. But to abet them in the murder of innocent lives? To think that the industry has stooped to this low, is totally beyond belief.

     

    26 May 2010 http://latimesblogs.latimes.com/greenspace/2010/05/gulf-oil-spill-top-kill-procedure-begins.html

    Engineers have begun the "top kill" maneuver aimed at stanching the gush of oil from a blown-out well at the bottom of the Gulf of Mexico, BP and U.S. Coast Guard confirmed. The much-awaited procedure began at 1 p.m. Central Daylight Time, according to BP. The maneuver, which BP officials warned could take hours or days to complete, would attempt to overpower the upward flow of oil by pumping drilling fluid -- and eventually a cement mixture -- at high pressure down the well. Several hundred engineers in Houston have prepped for the effort for weeks

     

    On 17 Aug 2010, in part 1 of the Ballistic analysis of the DWH-riser-wreck, I wrote:

    Video footage of the faulty BOP on top of Well A was only widely available to the public from June onwards. In a video dated 4 June 2010, an apparent “Dispersant Ops” Rov showed the BOP at 61.8 ft above seabed level, at 221.5 ft WNW of Well A location. Figure 3d confirmed our suspicion that the BOP had been “busily travelling” around instead of being Static at Well A as we had been led to believe.

     

    But how could one BOP stack be seen at so many places at any one time in the period beginning 20 April till at least the end of July 2010? If we piece all the little discrepancies together, there can only be the logical conclusions that:

    1. The original BOP at the 3rd well (S20BC) was blown off on 22 April 2010 (second more powerful underground blowout) as asserted by the Late Matts Simmons. Some sources even say the “never to be mentioned” second explosion that brought the DWH down was intentionally set off by one of the ROVs. A floating DWH rig would incriminate the perpetrators of this MIHOP disaster.

    2. BP secretly deployed another BOP stack (referred to as the FAKE BOP) at Well A, removed the broken riser on the original BOP and fixed on the the Fake BOP.

    3. Any of the ROV videos during this “critical” remove and reattached riser operation period would incriminate BP. That is the main reason BP cannot release any of the video footage of the ROV at work before June 2010.

    So this will mean there should be 3 BOP stacks altogether. First we have the Original BOP, then the FAKE BOP which was installed on well A in the aftermath of the blowout and retrieved on 3-4 September 2010 and the Replacement BOP which was eventually retrieved on 5 November 2010.

    We should be able to adduce the evidence from the following videos 160-1 to 160-4. I strongly advice readers to download the following You-tube ROV videos before they are completely “wiped off” from their respective websites.

    How do I know all these are true and accurate (if not in minute details at least the main story)? The proof is in the pudding. If I had been writing nonsense, would they have bothered to kill me along with the others from 24 Nov 2010 to July 2011?

    Incidentally, my wife and I should have been murdered on 24 Nov 2008 with fatal head wounds, cuts and bruises from the relentless battering by 4 personnel armed with 2 feet long machetes. Who could survive all that slashing and bounce back less than a week later, if not for the help of GOD? Incidentally, the life threats from the Oil Mafia started on 20 April 2008. Extremely coincidental isn't it? The oil mafia paid shills would have jumped on me long ago, if these dates were not true.

    There were serious attempts to eliminate me and my whole family in the first 6 months of 2011. Divine Guidance and of course the thousands of prayers around the world kept us safe. Unfortunately, in their desperate attempts to eliminate me, others were innocently poisoned or shot at. As with all covert murderous schemes, they cannot afford to have any eye-witnesses. In any case, the deaths of accidental eye-witnesses added to the confusion and planted misleading evidence. If all these sound familiar, it is. Look into all my past articles on the Art of Mass Deception practiced throughout the Gulf Disaster.

    To understand the ROV video footage of the BOPs, see figures 160a to 160c. Forget the fine details of the BOP stack. Look at the well-head connector, the frames and general layout of the BOP stacks. Each BOP stack is different. Essentially if the BOP stack raised onboard the Helix Q4000 on 5 Sept is different from the BOP stack seen in the video of the original BOP in June 2010, then you know for sure the Presidential Commission and all investigation reports based on the FAKE BOP are fundamentally wrong. So now you know what I had been talking about since July last year and the reason they need to secure my silence. Since I cannot be bought, my silence can only be secured through my demise.

    Lastly I wish to honour Bill Young, a former CIA agent living in Chiang Mai. He was murdered on 1 April 2011 in his home with a revolver in one hand and a cross in the other. I do not buy the suicide theory. How could the revolver and crucifix remained clutched in his hands after shooting himself? Like everything else, the revolver and crucifix were placed in his hands long after he was dead, to make it look like a suicide. He would rather die than betray GOD. God bless his soul. Amen.

    http://www.thefirstpost.co.uk/77251,people,news,cia-hitman-bill-william-young-found-dead-at-his-chiang-mai-home-air-america#ixzz1UMulZvFZ

    An American missionary's son who became a top CIA Vietnam War-era hit-man in the jungles of Burma, Laos and Thailand has been found dead in his Chiang Mai home, a bullet in his head, a revolver in one hand and a crucifix in the other.

     

    Video#160-1 of original BOP stack that blew off the third well (S20BC), fell to the seabed and was raised from the seabed on 3 July and held suspended for 13 days. The BOP was covertly dismantled and loaded onto one of the vessels and shipped off from site. Video and information - courtesy of Mr BeePee. Visit his website to see other videos. (could not load video link, click http to view)

          http://www.youtube.com/user/BeePeeOilDisaster#p/u/404/rbWZZiZVmTs

     

    Video#160-2 of FAKE BOP. Uploaded by X2YeZCAMCNC on Jun 9, 2010

    BP Gulf Oil Spill Leak Gusher 06-09-2010 03:46P BOP Subsea FlexJoint Cleaning BS Logo Removed

    In this narrated clip the ROV (remotely operated vehicle) is using the wire brush hydraulic tool to believe it or not remove the company logo (Oil States International Inc.- FlexJoint) plastered on the side of a part at the top of the damaged BOP (blowout preventer). Weird I just said that a few hours ago when I saw them getting this tool out, while joking. Don't they have better things to do.

    http://www.youtube.com/watch?v=A5mY_QNpspA 

    Video#160-3a-c of FAKE BOP being removed from the well-head at Well A from 3 to 4 September 2010. Compare the base of the BOP stack and well-head connector. Spot the huge differences.

    Video# 160-3a

    Recorded by JoseGerbils - Helix ESG Q4000 pulls the DWH BOP, weight gauge read 844,500 lbs

    http://www.youtube.com/watch?v=lgm6iUbaWCo&feature=related

    Video# 160-3b

    Recorded by Suzieconley – BOP removal Sept 3 2010

    http://www.youtube.com/watch?v=s0Y6BU_wfbY&feature=related

    Video# 160-3c

    FAKE BOP raised onboard the Helix ESG Q4000 on 4 Sept 2010.

    http://www.youtube.com/watch?v=hy8Zr46r7yA&feature=related

    Video#160-4 of Replacement BOP being removed from the well-head at Well A on 5 Nov 2010. Could not believe the stark difference? How on earth could the world's most highly paid, highly qualified professionals miss this crucial evidence? As Bernie Madoff said from his prison interview; “They had to know. But the attitude was sort of, ‘If you’re doing something wrong, we don’t want to know.’” What was that word again?.... Willful Blindness.

    Recorded by Moonofa – ... the end, my friend. Developer Driller II is unlatching and lifting its Blow Out Preventer from the BP Macondo well MC 252#1. Speed is 1x.

    http://www.youtube.com/watch?v=I3GgGRrTO4U&feature=related

  • Exactly a year ago, former White House energy advisor Carol Browner informed the world that 75% of the oil from the worst oil disaster in history had been cleaned up, evaporated and dispersed or burned off. “Mother Nature did her part,” Browner told the world.

    Don’t tell that to Cherri Foytlin, the oil worker’s wife and mother of six who walked from the Gulf to Washington for the one-year memorial of the BP blowout last April. The media has been largely silent since then, so Cherri and others decided they needed to remind people that “the oil is not gone.”

    Yesterday, protesters staged a protest at BP’s gleaming downtown New Orleans offices, where they dumped a batch of black gooey tar balls freshly hauled in from the beaches of Mississippi. After sitting in front of the BP's office building doorway for three hours as police tried to convince them to move, Cherri and two other protesters were arrested and booked for trespass later in the evening. But they had made their point.

  • Story Photo

    Fresh oil is surfacing all over the northern quadrant of the Gulf of Mexico. Reports of slicks that meander for miles and huge expanses of oil sheen that look like phantom islands are becoming common, again. Fresh oil, only slightly weathered, is washing ashore in areas hit hardest by last year’s massive spill, like Breton Island, Ship Island, the Chandeleurs and northern Barataria Bay. BP has reactivated its Vessels of Opportunity (VoO) program to handle cleanup. It’s a sickeningly familiar scene that has fishermen, researchers and public officials searching for answers, as haunting memories of last year’s calamity come roaring back.

    The fifty-thousand-dollar question, of course, is where is all the new oil coming from?

  • BP's permit to drill Macondo well was submitted to MMS on 10 March 2009

    These videos talking about "something wicked (a depopulation event)" about to happen. Mexico was mentioned many times with reference to the Aztec human sacrifice. They were speculating on a volcanic eruption of some sort. Coincidentally the radio interviews were 20 and 28 of April 2009. So words must have leaked out but details were fuzzy; leaving room for a lot of speculation. Look for the keywords like mass destruction, vaccine, population reduction, mexico etc.

    The Macondo well was destined to blow up in Nov 2009 but Hurricane Ida spoiled the plan. The April 2010 blowout event was a backup plan, a retry.

  • Story Photo
    • by BK Lim (first written on 10 Aug 2010, revised on 28 April 2011)

    The first few obvious discrepancies to stick out like a sore thumb were the “2 major leaks on the riser” substitution for the real leaks on the seabed. These discrepancies were first raised in the forensic analysis of the Deepwater Horizon wreckage (DWH blowout CSI: Why-it-could-not-have-happened-as-reported-by-BP ) in July 2010.

    In figure 157-1, these discrepancies are illustrated diagrammatically. BP's official story on the leaks on the riser are given in figures 157-2 and 157-3. Till this day, none of the main stream media had ever questioned the flaws in BP's story of the two leaks on the riser. One year later, we again bring up the discrepancies to illustrate the physical impossibilities.

    To refresh readers, BP claimed that the BOP was largely intact and still standing after the DWH sank on 22 April 2010. The 5,000ft riser was bent but still connected to the BOP at well A. BP claimed that all the oil spilled into the gulf came from two leaks on the riser. The first (1) were several punctures sustained on the riser when it bent as the DWH sank. The second (2) and bigger leak was the severed end of the “riser” 480 ft north of well A. Rov videos and images of the second leak were shown first in early May 2010. The first leak (1) on top of the BOP was only shown weeks later.

    Discrepancy #1

    It is obvious that the severed casing at 2 had not been bent, twisted and broken off during the sinking of the DWH. If it was, the casing could not have maintained its almost circular shape. It appears more likely to have been either cut or torn-off as in “blown apart”. This itself rules out the severed casing being the mid section of the riser since there would not be any reason for the riser to be blown apart anywhere in its mid section.

    Discrepancy #2

    The diameter of the casing at 2 is evidently much larger than the diameter of the bent riser at 1. They do not appear to look the same at all. The casing at 2 appears more likely to be part of the casing coming directly out of the seabed than being connected to the riser coming from the top of the BOP.

    Discrepancy #3

    Assuming BP's official version, how can the second leak (480 ft away from the BOP) have a large volume of oil/gas flow than the first leak (1) directly on top of the BOP? If the oil and gas were flowing out of the same riser pipe, should not the first leak be the larger of the two?

    Discrepancy #4

    Leak (1) is about 70 ft above the seabed. Could oil and gas flow downwards past the punctured bend at 1 to reach the second leak 480 ft away at seabed level? If some oil and gas did leak through (1), then leak 2 should be spewing less oil and gas than leak (1) – see discrepancy #3. But even BP admitted leak 2 to be the large of the two.

    Discrepancy #5

    Leak 2 appeared in all videos and images to spew more oil than gas and with more ferocity than leak (1). How can that be when all the pressure would have leaked out at (1)?

    Discrepancy #6

    Well A and the BOP was south of the second leak location. So if well A was the source, the oil and gas would have flowed northwards. But in all the rov videos, the casing was coming out of the seabed from the north with the oil and gas flowing southwards. So where is the connection?

    There are many more discrepancies but the few that I have listed above should be enough to completely refute the official version of 2 leaks on the riser coming out of the BOP at well A. For what reasons must BP lie so blatantly on the 2 leaks on the seabed?

  • Story Photo
  • But is the industry truly ready to go back to work? A couple of points make one uncertain. For starters, assurances that BP was the only bad actor aren't good enough, and verge on the naïve -- all actors in the Gulf knew or should have known that any accident by anyone would affect all.

    What about the spill containment equipment? As described, this is an impressive bit of work. Yet it also has a distinct political quality -- in order to get working again in the United States, the industry was forced to take such action; otherwise no one would be convinced it is serious about the environment. But we see no word of such equipment being deployed elsewhere in the deepwater world, such as in Angola, Brazil, Canada, Nigeria and Norway. Are we to believe that the Gulf of Mexico is the only place at risk of a big spill?

  • Story Photo
    • by BK Lim (23 Feb 2011) email: bklimgeohazards@gmail.com

    Is there a common factor between the quake off Fort Morgan on 18 Feb 2010 and the recent swarm of quakes occurring in the vicinity of the New Madrid Fault zone? You are right if the BP Mega Oil spill and the Deepwater Horizon blowout on 20 April 2010 comes to mind.

    They are all quakes similar to the disastrous 22 Feb 2011 quake that occured close to Christshurch in New Zealand. Their shallow epicentres are off the main tectonic (or intra-plate) main fault lines. There are significant differences though, especially in magnitude and tectonic plate settings. The recent NZ disaster was more devastating than an earlier quake 11 times more powerful with its epicentre on the plate margin.

    Since the 2Aug 2010 quake at Louisiana, we have been warning of more occurrences of such shallow low magnitude quakes. See figure 145-1 which shows some of the hidden series of NW-SE strike-slip fault lines typical of intra-plate movement. The fault chart (prepared in August and updated only with annotations) was only published on 10 Nov2010, Update On BP Rigs Location & the Fault Connection. The consequence of the continuing corosive erosion along these faults by leaking hydrocarbons from deep reservoirs (not only from the Macondo prospect) is the release in stresses between the upper and lower crust; resulting in shallow quakes of generally low magnitude. This was mentioned in a recent article, first written on 14 Feb and updated 20 Feb 2011.

    ~~~start of quote~~~Silencing The Independent Voices Of Truth On The BP's Mega Oil Spill GOM

    For millions of years, the south-eastern part of the North American tectonic plate (south-east of the New Madrid Fault line) has been thrusting in a north-easterly direction while the western half of the plate has been moving south along the San Andreas fault line. This is the main reason for the present gulf seabed morphology.

    The resultant torsion tension is reflected by the fault pattern illustrated in a previous article BP's Rigs Location & Fault Connection. Besides lateral stresses, vertical stresses also developed between the upper and lower section of the tectonic blocks due to differential upper and lower slide movement. The abnormal occurrences of hundreds of shallow and low magnitude earthquakes since the Macondo blowout are the direct consequence of the continual release of these pent-up stress zones. FEMA recently sent out RFI (request for information) to identify vendors for the emergency supply of food rations, various fuels and hydration in support of disaster relief efforts based on a catastrophic disaster event within the New Madrid Fault system for a survivor population of 7 million to be utilised for the sustainment of life during a 10-day period of operations. Is FEMA having privileged information of an impending disaster in the New Madrid Fault area, 9 months after the BP's Mega-oil Spill disaster?

    ~~~end of quote ~~~~

    What is the area extent of these continuing leakages of hydrocarbons along these faults , vaporisation of methane hydrates due to warming effect of these leaking hydrocarbons and rapid mass depletion caused by continuing sub-seabed erosion? Judging by the number of reported quake-swarms, we are pretty close to the point of no return if we have not passed that point yet.

    So far the quakes had been low magnitude between 2 to 4 on the Richter Scale. FEMA is expecting a major quake disaster similar to the recent Christchurch Quake in New Zealand. As we have seen, the shallow quakes are more devastating than a deep one at the base of the crust. The New Madrid Fault is an intra-plate tectonically stressed zone. It behaves very differently from the tectonic plate margins.

    Since these shallow intra-plate quakes had been unleashed by the drilling and blowouts at the Macondo prospect, it makes sense to monitor closely the seafloor and the continental shelf edges. Mapping the gas vents in the vicinity of these faults and shelf edges would go a long way to making accurate predictions of what to expect in the vicinity of the New Madrid Fault zone. More powerful need not necessarily be more devastating but one thing for sure, the disaster has not ended yet despite what you have been told. Christchurch was hit by a hidden fault (???)

    ~~~ start of quote ~~~~

    New_Zealand_Earthquake_Science By ALICIA CHANG, AP Science Writer–Tue Feb22, 6:10pmET

    No one died in that early morning quake — which was 11 times stronger — mainly because it was centered farther away, about 30 miles west of the city center. It was also twice as deep as Tuesday's aftershock. Shallower quakes tend to be more damaging.

    LOS ANGELES – The latest New Zealand earthquake was a deadly combination of distance, depth and timing. While weaker than the one that rocked the area last September, it did more damage and cost lives, primarily because of its location. Tuesday's magnitude-6.3 quake was centered about 3 miles from the populated hub of Christchurch, toppling buildings, killing dozens and trapping others. It was also only about 3 miles deep and occurred during the middle of a workday when commercial buildings were filled with employees.The jolt "is squarely beneath the city itself," said seismologist Egill Hauksson of the California Institute of Technology. "All the old historic buildings are being shaken more violently than they were built to withstand." Scientists classified it as an aftershock of the powerful magnitude-7 that struck last Sept. 4.

  • The recently published National Commission Report to the President of the United States of America (11th January 2011) and BP's own earlier Accident Investigation Report dated 8th September 2010 have focused almost entirely on the failings of equipment and processes on the drilldeck of the Deepwater Horizon, on the seafloor BOP and associated equipment and on the errors and mistakes made in drilling and cementing up of the close to completed well.

    The fact is that BP were drilling at Macondo MC 252 in an area of well known and documented geological hazards (known in the industry as "Geohazards"). At Macondo these included such features as extensive beds of frozen gas (or methane hydrates) and a number of layers of artesian overpressured sands where the interstitial natural water pressures could cause casing collapse due to disturbance of those sands. This process is known as "liquefaction", also known in the trade as "shallow water flows" [SWF]. The presence of gas hydrates and shallow water flows in this Mississippi canyon shelf edge zone is very well documented by the MMS, BP and other operators.

  • Story Photo

    As we have seen in many cases, disasters can be highly profitable for those who know in advance or “privileged few in the know” (PFitK). This is very clear from the pattern of massive selling by BP’s directors and Goldman Sachs before the advent of an impending disaster. See A pattern of massive shares sell-off by BP directors prior to expected disasters.

    Though hard to believe, there are many who would profit without hesitation upon the miseries of others. A mega-disaster like the BP’s Oil Spill is one of those. Sometimes it is hard to say if a prescribed cure is supposed to make you feel better or improve the bottom line of the one prescribing it. Time will always tell, as it is revealing in the case of the BP Gulf Oil disaster.

    Just as it would be highly improper for surgeons to mislead on the medical procedures, BP the “doctor” should lose its “medical license” and be held criminally liable for deliberate misleading information on so many occasions. Six months later, NOAA and the Presidential Investigative Panel should have been able to evaluate not only the effectiveness of the medicine prescribed but also the manner it was administered. If these regulatory bodies are still sleeping on their job after six months, then either delinquency or corruption has already set in.

    By most accounts BP, NOAA and all the regulatory bodies fared poorly in this disaster. Later postings will delve into the technological and geological aspects. In this posting, we will concentrate on the question whether the post-disaster recovery program had become a profitable scam. It goes without saying that BP as an organization would suffer hefty financial losses not monetary gains. That would make it all the more; much “safer” for the privileged few to profit personally. Evidence of profit motives in the post-disaster recovery efforts would substantiate earlier suspicions that this disaster had been allowed to happen.

    It is an undeniable fact that corners are cut everyday across the globe in almost every sector of human societies. Of all the industries, the offshore oil industry is the most regulated with the most stringent HSE policies. Hence it is logically impossible for a potential mega disaster to sail through the elaborate screening “Check & Balance” process. Unlike wildcat drillings in the pre-seventies, every location to be drilled had to be evaluated with respect to exploration and production objectives, shallow geohazards, seabed and logistics problems. That is why few mega-disasters occurred even though near-misses and accidents do occur on a daily basis. By all accounts, this disaster could have been averted. Yet it was allowed to happen. Why?

    Obviously there must be a profit motive, not for BP but for the PFitK. Having established this fact we will proceed to examine the deliberate misleading information BP has been giving recently. In every post-disaster recovery efforts, there is the right way and the wrong way. No crime is committed even if the wrong (but profitable) way was deliberately chosen. There is no lack of senseless recovery works that can be carried out without contributing anything to the recovery or the welfare of the Gulf Victims (environment, people and marine wildlife). Readers can contribute more examples but for now we concentrate on the high cost items.

    Four Drilling Rigs at Site

    We can argue until the cows come home on BP’s intentions but does BP really need four expensive rigs at the cost of 0.5 to 1 million USD/day at the Macondo site? Even if they need to drill more wells (relief or otherwise) it would stretch resources to the hilt with 5 wells going together within the same site. But if the intention is to chalk up tax-deductible expenses for the idling rigs then it made sense. No wonder the recovery costs keep ballooning especially in early November with an additional 7.7 billion USD.

    Normal exploration budgets are guided by precedence. In a mega disaster, there is virtually no cost control. Would BP exploit the disaster to dump all their idling rigs into the Macondo site? You bet BP will, given its opportunistic instincts. BP’s unfortunate partners (Mitsui and Anadarko) will have to foot 10% and 25% respectively. Few would dare to question the need for four drilling rigs under classified disaster circumstances. Is that why the Live Feed from West Sirius ROV1 is still shown on BP’s website even though West Sirius had moved out of the Macondo site to park at the edge of Mississippi Canyon, south of Grand Isle? Obviously the ROV1 cannot be deployed from West Sirius to work at the Macondo site 165km away. Alternatively if the ROV1 is working at the Mississippi Canyon (for whatever reasons), the daily operation cost of West Sirius cannot be charged to the Macondo Post-Disaster Recovery Program (MPDRP). Any responsible corporate would not cheat and evade tax on an unfortunate disaster.

    It would probably look less absurd if West Sirius is sitting within the Macondo Site. It however, moved out less than a week (3 NOV) after an earlier posting (A New Drilling Rig At Macondo Site) questioned the need for 4 drilling rigs to be stationed so close to each other. Drilling rigs normally work in isolation with support vessels. This was strange when Well A was already declared capped in mid July and permanently killed in mid Sept by DD3 at Relief Well C.

    There was not much news on DD2 at Relief Well D. Industry’s experts were surprised when BP spared no efforts to drill 2 relief wells when one should be sufficient. Anyone questioning the need for two relief wells in May would have been scorned, if not “executed”in the press. This is the unconstrained purchasing power of any disaster; 911, Afghan War, Iraqi War or any disaster-relief efforts. You question, you die either by character assassination or … !

    Anyway it was thought to be a good PR move, to show the world that BP would spare no effort to contain the spill. Those with the “evil thoughts” that BP could be fielding the additional drilling rig to pad up the MPDRP expenses had to hold their tongues and wait to be vindicated. But when the Discovery Enterprise (DE) was added on and all the 3 rigs (DE, DD2 and DD3) did not demobilize from site after the completion of the relief wells, the suspicion firmed up. When the West Sirius moved in, all doubts were erased.

    Drilling rigs that do not drill offer many corrupt opportunities. With skeletal maintenance crew and cooperation between the operation managers of BP and contractors, the lure to “capitalize” on operational costs for unused operation workers is just too high to ignore. Even at the minimum average of 500 USD/day/worker for 100 workers works out to be 1,500,000 USD/month per rig. This common scam of fielding virtual workers is undetectable by outside parties except the most diligent accountant / QC consultant.

    Materials, consumables and disposable instruments offer abundant opportunities for site managers to cooperate with suppliers to cheat. Besides wastage, the important question is “Are some of the work at site warranted or merely to line up the pocket?” It is virtually impossible to QC the volume needed to grout the seafloor, notwithstanding whether they were effective or necessary. Like virtual workers, the reported amount consumed could actually be more than triple the actual amount used. No wonder contractors, body shops and suppliers laughed their way to the bank and workers paid handsomely with bonuses do not talk.

    If anyone has any doubt in this, just look up the drilling rig position at www.marinetraffic.com. For months tracking the drilling rigs’ position was never a problem. A week after A New Drilling Rig At Macondo Site was posted on 31 Oct, the position of these rigs went haywire. DE was flung (virtually) to Lake Superior, DD2 to South Pacific and DD3 to Arctic, Africa and South Pacific. It is hilarious that BP would control www.marinetraffic.com website to adulterate the satellite position. These position anomalies just confirmed the accuracy of this report and our previously reported ROV coordinates adulteration. It also confirms BP’s record spending on buying up websites like The Oil Drum and bloggers so that they speak kindly of BP in spite of BP’s evil deeds. No wonder the main media all over the world speak with one silence voice on BP’s evil ways. Now you understand.

    So when BP says “We Are Here To Stay And Make Things Right”, they probably meant it wholeheartedly. Who wouldn’t? With impunity for causing any disaster (Alaska pipeline, Texas Refinery, Macondo and future) life is good for BP in America when they make things right (for themselves).

  • E-mails and letters obtained by ProPublica show that the main contractor BP was using to check its facilities, Acuren, employed inspectors who weren't certified to perform their jobs and may not have been properly trained. The certification issues affected at least 19 inspectors responsible for more than 13,000 locations along the line and were serious enough that they were reported to BP's board of directors in London.

    Pascal, a career Environmental Protection Agency attorney only seven weeks into her retirement, knew as much as anyone in the federal government about BP, the company that owned the well. She understood in an instant what it would take others months to grasp: In BP's 15-year quest to compete with the world's biggest oil companies, its managers had become deaf to risk and systematically gambled with safety at hundreds of facilities and with thousands of employees' lives.

    This is an excellent "Must Read" article to understand the BP's disaster.

  • About this Author
    Vineacity
    Articles Posted: 90
    Links Seeded: 281
    Member Since: 7/2010
    Last Seen: 2/22/2012
    Happy to contribute and share my 30 years work experience and knowledge as a geohazards specialist towards averting geohazards disasters.

    Follow BK Lim to get e-mail or watchlist alerts whenever new content is published, or subscribe via RSS:

    RSS
    BK Lim's Watchlist

    Groups & Authors:

    • (none)

    Tags & Regions:

    • (none)

    BK Lim's Private Content
    BK Lim has not published any private articles, seeds, or discussions that you have access to.
    BK Lim's Latest Comments